HL incident on 2020-05-13 — TX

Operator
Dapl-Etco Operations Management, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2020-05-13 08:12
Report number
Location
TX
Narrative
On 5/13/20 at 08:12 control center received an lel alarm from the johnson's corner pump station. The station was immediately shutdown. Controller contacted local field operations management to investigate. Upon investigation an approximate 4.6 barrel release from failed 1/2"stainless steel tubing was identified. All free product was contained within the pump building on the concrete floor and was picked up with a vac truck and absorbent pads. The failed tubing was part of a thermal relief system between the pump discharge check valve and gate valve. This tubing was mounted in a fixed overhead position which did not allow for movement and thermal fluctuations over time stressed the tubing to fail at the fitting. The tubing was replaced and the pump station returned to service. Common designs at other pump stations on the system were inspected for similar condition and addressed as needed. To prevent recurrence, the thermal relief tubing will be brought down from the overhead fixed location and re positioned in a manner that will be supported but also allow for movement due to thermal fluctuations which will prevent undue stresses being imparted on the tubing and associated fittings. This will also be completed at all other pump stations on the system with common design.
Detailed record list
Report Received Date
2020-06-12 00:00:00
Iyear
2020
Report Number
20200174
Supplemental Number
33920
Report Type
Supplemental Final
Operator Id
Name
Dapl-Etco Operations Management, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-05-13 08:12:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4.6
Recovered Bbls
4.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2020-05-13 08:12:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-05-13 08:12:00
Restart Datetime
2020-05-13 16:40:00
On Site Datetime
2020-05-13 08:12:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Johnsons Corner Pump Station
Segment Name
29004 - 30" Watford City To Patoka
Onshore State Abbreviation
Nd
Onshore Postal Code
58847
Onshore City Name
Johnsons Corner
Onshore County Name
Mckenzie
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
1/2" Stainless Steel Tubing
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
12
Est Cost Prop Damage
50
Est Cost Emergency
1470
Est Cost Environmental
0
Est Cost Other
0
Prpty
1532
Accident Psig
509
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the incident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Small Diameter Stainless Steel Tubing Failure (Crack) At Fitting Interface Due To Thermal Stressing.
Additional Thermal Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2020-06-18 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
T************@e*************.com
Narrative
On 5/13/20 at 08:12 control center received an lel alarm from the johnson's corner pump station. The station was immediately shutdown. Controller contacted local field operations management to investigate. Upon investigation an approximate 4.6 barrel release from failed 1/2"stainless steel tubing was identified. All free product was contained within the pump building on the concrete floor and was picked up with a vac truck and absorbent pads. The failed tubing was part of a thermal relief system between the pump discharge check valve and gate valve. This tubing was mounted in a fixed overhead position which did not allow for movement and thermal fluctuations over time stressed the tubing to fail at the fitting. The tubing was replaced and the pump station returned to service. Common designs at other pump stations on the system were inspected for similar condition and addressed as needed. To prevent recurrence, the thermal relief tubing will be brought down from the overhead fixed location and re positioned in a manner that will be supported but also allow for movement due to thermal fluctuations which will prevent undue stresses being imparted on the tubing and associated fittings. This will also be completed at all other pump stations on the system with common design.
Report Received Date 2020-06-12 00:00:00
Iyear 2020
Report Number 20200174
Supplemental Number 33920
Report Type Supplemental Final
Operator Id 39205 PHMSA Enforcement
Name Dapl-Etco Operations Management, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-05-13 08:12:00
Location Latitude 47.79933 Google Maps OpenStreetMap
Location Longitude -102.9238 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4.6
Recovered Bbls 4.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2020-05-13 08:12:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-05-13 08:12:00
Restart Datetime 2020-05-13 16:40:00
On Site Datetime 2020-05-13 08:12:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Johnsons Corner Pump Station
Segment Name 29004 - 30" Watford City To Patoka
Onshore State Abbreviation Nd
Onshore Postal Code 58847
Onshore City Name Johnsons Corner
Onshore County Name Mckenzie
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details 1/2" Stainless Steel Tubing
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 12
Est Cost Prop Damage 50
Est Cost Emergency 1470
Est Cost Environmental 0
Est Cost Other 0
Prpty 1532
Accident Psig 509
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the incident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Small Diameter Stainless Steel Tubing Failure (Crack) At Fitting Interface Due To Thermal Stressing.
Additional Thermal Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2020-06-18 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Regulatory Compliance
Authorizer Email T************@e*************.com
Narrative On 5/13/20 at 08:12 control center received an lel alarm from the johnson's corner pump station. The station was immediately shutdown. Controller contacted local field operations management to investigate. Upon investigation an approximate 4.6 barrel release from failed 1/2"stainless steel tubing was identified. All free product was contained within the pump building on the concrete floor and was picked up with a vac truck and absorbent pads. The failed tubing was part of a thermal relief system between the pump discharge check valve and gate valve. This tubing was mounted in a fixed overhead position which did not allow for movement and thermal fluctuations over time stressed the tubing to fail at the fitting. The tubing was replaced and the pump station returned to service. Common designs at other pump stations on the system were inspected for similar condition and addressed as needed. To prevent recurrence, the thermal relief tubing will be brought down from the overhead fixed location and re positioned in a manner that will be supported but also allow for movement due to thermal fluctuations which will prevent undue stresses being imparted on the tubing and associated fittings. This will also be completed at all other pump stations on the system with common design.

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