HL incident on 2020-05-06 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$184,720
Incident datetime
2020-05-06 12:45
Report number
Location
TX
Narrative
On may 6, 2020 at 12:45 pm cdt, product was visible near the line 1 mp 801 valve by the technician when he arrived at the valve site to complete scheduled maintenance. The edmonton control center was contacted and the line was shut down to investigate. Additional crews were dispatched to determine the source of the product. After removing standing water and excavating the area, it was discovered that the seal packing pipes had cracked causing approximately 1 cup of crude oil to be released. The internal investigation determined that frost heave caused the piping to crack. On the evening of may 8, 2020 the plan to replace the piping was finalized and it was determined that the costs for repair and clean up would meet the requirement for an nrc notification. The nrc was notified at 9:05 pm cdt (#1276936). On may 9, 2020 the seal packing and body bleep piping was replaced and the line placed back into service at 2:35 am cdt. A 48-hour update to the nrc was made on may 10, 2020 at 4:35 pm cdt (#1277006). Upon completing the valve repair and in an effort to remediate the impacts, enbridge performed additional excavation activities to address the release. Preliminary excavation resulted in the discovery of impacted soils in unanticipated locations. Consequently, enbridge has initiated a site investigation designed to further assess potential impacts from the valve release as well as potential previous impacts. The goal remains to remediate to applicable environmental standards with the possibility of additional excavation. Due to the remote location of the site, costs are inflated for dispatching qualified professionals to perform investigatory work and impacted materials must be transported great distances for disposal at permitted facilities. The actual volume released at mp 801 was 0.0015 barrels. The PHMSA portal does not recognize volumes less than 0.1 barrels therefore that is the volume entered.
Detailed record list
Report Received Date
2020-06-05 00:00:00
Iyear
2020
Report Number
20200167
Supplemental Number
33867
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2020-05-06 12:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-05-06 12:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-05-06 12:55:00
Restart Datetime
2020-05-09 02:35:00
On Site Datetime
2020-05-06 12:45:00
Nrc Rpt Datetime
2020-05-08 21:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Line 1
Segment Name
Mp 801
Onshore State Abbreviation
Nd
Onshore Postal Code
58225
Onshore City Name
Drayton
Onshore County Name
Pembina
Designated Location
Milepost/valve Station
Designated Name
801
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M&j (Spx Flow)
Installation Year
1997
Manufactured Year
1994
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1
Est Cost Prop Damage
184720
Est Cost Emergency
57
Est Cost Environmental
45000
Est Cost Other
0
Prpty
229778
Accident Psig
999
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
71016
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
Investigation Did Not Yield Results That Indicated Any Controller Contribution (Field Identified The Leak)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Frost Heave
Nf Extreme Weather Ind
No
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2020-06-05 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On may 6, 2020 at 12:45 pm cdt, product was visible near the line 1 mp 801 valve by the technician when he arrived at the valve site to complete scheduled maintenance. The edmonton control center was contacted and the line was shut down to investigate. Additional crews were dispatched to determine the source of the product. After removing standing water and excavating the area, it was discovered that the seal packing pipes had cracked causing approximately 1 cup of crude oil to be released. The internal investigation determined that frost heave caused the piping to crack. On the evening of may 8, 2020 the plan to replace the piping was finalized and it was determined that the costs for repair and clean up would meet the requirement for an nrc notification. The nrc was notified at 9:05 pm cdt (#1276936). On may 9, 2020 the seal packing and body bleep piping was replaced and the line placed back into service at 2:35 am cdt. A 48-hour update to the nrc was made on may 10, 2020 at 4:35 pm cdt (#1277006). Upon completing the valve repair and in an effort to remediate the impacts, enbridge performed additional excavation activities to address the release. Preliminary excavation resulted in the discovery of impacted soils in unanticipated locations. Consequently, enbridge has initiated a site investigation designed to further assess potential impacts from the valve release as well as potential previous impacts. The goal remains to remediate to applicable environmental standards with the possibility of additional excavation. Due to the remote location of the site, costs are inflated for dispatching qualified professionals to perform investigatory work and impacted materials must be transported great distances for disposal at permitted facilities. The actual volume released at mp 801 was 0.0015 barrels. The PHMSA portal does not recognize volumes less than 0.1 barrels therefore that is the volume entered.
Report Received Date 2020-06-05 00:00:00
Iyear 2020
Report Number 20200167
Supplemental Number 33867
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2020-05-06 12:45:00
Location Latitude 48.712069 Google Maps OpenStreetMap
Location Longitude -97.123908 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-05-06 12:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-05-06 12:55:00
Restart Datetime 2020-05-09 02:35:00
On Site Datetime 2020-05-06 12:45:00
Nrc Rpt Datetime 2020-05-08 21:05:00
Nrc Rpt Num 1276936 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Line 1
Segment Name Mp 801
Onshore State Abbreviation Nd
Onshore Postal Code 58225
Onshore City Name Drayton
Onshore County Name Pembina
Designated Location Milepost/valve Station
Designated Name 801
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M&j (Spx Flow)
Installation Year 1997
Manufactured Year 1994
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1
Est Cost Prop Damage 184720
Est Cost Emergency 57
Est Cost Environmental 45000
Est Cost Other 0
Prpty 229778
Accident Psig 999
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 71016
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details Investigation Did Not Yield Results That Indicated Any Controller Contribution (Field Identified The Leak)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Frost Heave
Nf Extreme Weather Ind No
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2020-06-05 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On may 6, 2020 at 12:45 pm cdt, product was visible near the line 1 mp 801 valve by the technician when he arrived at the valve site to complete scheduled maintenance. The edmonton control center was contacted and the line was shut down to investigate. Additional crews were dispatched to determine the source of the product. After removing standing water and excavating the area, it was discovered that the seal packing pipes had cracked causing approximately 1 cup of crude oil to be released. The internal investigation determined that frost heave caused the piping to crack. On the evening of may 8, 2020 the plan to replace the piping was finalized and it was determined that the costs for repair and clean up would meet the requirement for an nrc notification. The nrc was notified at 9:05 pm cdt (#1276936). On may 9, 2020 the seal packing and body bleep piping was replaced and the line placed back into service at 2:35 am cdt. A 48-hour update to the nrc was made on may 10, 2020 at 4:35 pm cdt (#1277006). Upon completing the valve repair and in an effort to remediate the impacts, enbridge performed additional excavation activities to address the release. Preliminary excavation resulted in the discovery of impacted soils in unanticipated locations. Consequently, enbridge has initiated a site investigation designed to further assess potential impacts from the valve release as well as potential previous impacts. The goal remains to remediate to applicable environmental standards with the possibility of additional excavation. Due to the remote location of the site, costs are inflated for dispatching qualified professionals to perform investigatory work and impacted materials must be transported great distances for disposal at permitted facilities. The actual volume released at mp 801 was 0.0015 barrels. The PHMSA portal does not recognize volumes less than 0.1 barrels therefore that is the volume entered.

All rights reserved. Copyright © by ClearPHMSA