Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2020-05-04 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2020-05-04 14:00
Report number
Location
OK
Narrative
At 14:00 on 5/4/2020, magellan personnel identified product being released from a small diameter check valve relief on the product sampler system. The check valve was immediately isolated and clean-up of impacted soil was initiated. Upon investigation of the cause of the incident, it was discovered that the check valve relief was not adequately piped to the sump during installation on march 31, 2020. Following the release, the check valve relief was properly piped to the sump to mitigate future occurrence and the pre-startup safety review procedure was reviewed with the affected employee.
Detailed record list
Report Received Date
2020-06-03 00:00:00
Iyear
2020
Report Number
20200158
Supplemental Number
33847
Report Type
Original Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2020-05-04 14:00:00
Location Latitude
36.130179
Location Longitude
-96.028425
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
7
Recovered Bbls
7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-05-04 14:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Was Immediately Isolated, Shut Down Of The Facility Was Not Required
On Site Datetime
2020-05-04 14:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
West Tulsa Explorer
Segment Name
Sta. No. 503
Onshore State Abbreviation
Ok
Onshore Postal Code
74107
Onshore City Name
Tulsa
Onshore County Name
Tulsa
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
2020
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Relief Not Pumped To Sump
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
0
Est Cost Emergency
34000
Est Cost Environmental
0
Est Cost Other
0
Prpty
34300
Accident Psig
60
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The explorer change shack is not tied into our scada or cpm systems
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-06-03 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 14:00 on 5/4/2020, magellan personnel identified product being released from a small diameter check valve relief on the product sampler system. The check valve was immediately isolated and clean-up of impacted soil was initiated. Upon investigation of the cause of the incident, it was discovered that the check valve relief was not adequately piped to the sump during installation on march 31, 2020. Following the release, the check valve relief was properly piped to the sump to mitigate future occurrence and the pre-startup safety review procedure was reviewed with the affected employee.
| Report Received Date | 2020-06-03 00:00:00 |
|---|---|
| Iyear | 2020 |
| Report Number | 20200158 |
| Supplemental Number | 33847 |
| Report Type | Original Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2020-05-04 14:00:00 |
| Location Latitude | 36.130179 Google Maps OpenStreetMap |
| Location Longitude | -96.028425 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 7 |
| Recovered Bbls | 7 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2020-05-04 14:00:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Release Was Immediately Isolated, Shut Down Of The Facility Was Not Required |
| On Site Datetime | 2020-05-04 14:00:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | West Tulsa Explorer |
| Segment Name | Sta. No. 503 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74107 |
| Onshore City Name | Tulsa |
| Onshore County Name | Tulsa |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Auxiliary Piping (E.g. Drain Lines) |
| Installation Year | 2020 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Stainless Steel |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Relief Not Pumped To Sump |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 300 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 34000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 34300 |
| Accident Psig | 60 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The explorer change shack is not tied into our scada or cpm systems |
| Employee Drug Test Ind | Yes |
| Contractor Drug Test Ind | No |
| Num Employees Tested | 1 |
| Num Employees Failed | 0 |
| Cause | Incorrect Operation |
| Cause Details | Equipment Not Installed Properly |
| Operation Type | Equipment Not Installed Properly |
| Related Failure Follow Ind | Yes |
| Category Type | Construction |
| Operator Qualification Ind | No |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2020-06-03 00:00:00 |
| Authorizer Name | G**** R**** |
| Authorizer Telephone | 918-574-7165 |
| Authorizer Title | Supervisor Integrity Management |
| Authorizer Email | G**********@m*********.com |
| Narrative | At 14:00 on 5/4/2020, magellan personnel identified product being released from a small diameter check valve relief on the product sampler system. The check valve was immediately isolated and clean-up of impacted soil was initiated. Upon investigation of the cause of the incident, it was discovered that the check valve relief was not adequately piped to the sump during installation on march 31, 2020. Following the release, the check valve relief was properly piped to the sump to mitigate future occurrence and the pre-startup safety review procedure was reviewed with the affected employee. |
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