HL incident on 2020-04-24 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-04-24 11:40
Report number
Location
TX
Narrative
On 04/24/20 at 11:40, enterprise technician during station rounds discovered crude leaking on the ground from the bottom side of oth1 pipeline at the south manifold. The pipeline was isolated and a plidco clamp was installed. The pipeline was restored to its predefined level of service. Approximately 40 barrels was released inside the dike wall containment area. To prevent recurrence, this segment will be placed into quarterly dead leg flush program. All soil was remediated. Initial nrc call was made april 24, 2020 at 13:12 nrc# 1276009. The 48 hour update was placed april 26 at 10:56 nrc #1276115. Trrc was notified on 04/24/2020 at 12:11, incident # 2192.
Detailed record list
Report Received Date
2020-05-19 00:00:00
Iyear
2020
Report Number
20200143
Supplemental Number
34098
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-04-24 11:40:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
40
Recovered Bbls
40
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2020-04-24 11:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-04-24 11:40:00
Restart Datetime
2020-04-25 22:55:00
On Site Datetime
2020-04-24 11:40:00
Nrc Rpt Datetime
2020-04-24 13:12:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Appelt South Manifold
Segment Name
Lid: Oth1
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Station: 4+35
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Aboveground Mainline Piping
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Husteel Co.
Pipe Coating Type
Paint
Installation Year
2014
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
70000
Est Cost Other
338521
Est Cost Other Details
Osro; Other Costs Associated With Clean Up (Roll Off Boxes, Vacuum Boxes, Etc.)
Prpty
409021
Accident Psig
170
Mop Psig
590
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
27984
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release happened due to corrosion.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Other
Int Visual Exam Details
Pin Hole
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
0600 Orientation
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2016
Hydrtst Most Rcnt Pressure
761
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Y******* B**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
Y***@e****.com
Preparer Telephone
713-9068726
Prepared Date
2020-08-04 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
281-684-8179
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
On 04/24/20 at 11:40, enterprise technician during station rounds discovered crude leaking on the ground from the bottom side of oth1 pipeline at the south manifold. The pipeline was isolated and a plidco clamp was installed. The pipeline was restored to its predefined level of service. Approximately 40 barrels was released inside the dike wall containment area. To prevent recurrence, this segment will be placed into quarterly dead leg flush program. All soil was remediated. Initial nrc call was made april 24, 2020 at 13:12 nrc# 1276009. The 48 hour update was placed april 26 at 10:56 nrc #1276115. Trrc was notified on 04/24/2020 at 12:11, incident # 2192.
Report Received Date 2020-05-19 00:00:00
Iyear 2020
Report Number 20200143
Supplemental Number 34098
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-04-24 11:40:00
Location Latitude 29.7554 Google Maps OpenStreetMap
Location Longitude -95.1446 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 40
Recovered Bbls 40
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2020-04-24 11:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-04-24 11:40:00
Restart Datetime 2020-04-25 22:55:00
On Site Datetime 2020-04-24 11:40:00
Nrc Rpt Datetime 2020-04-24 13:12:00
Nrc Rpt Num 1276009 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Appelt South Manifold
Segment Name Lid: Oth1
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Station: 4+35
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Aboveground Mainline Piping
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Husteel Co.
Pipe Coating Type Paint
Installation Year 2014
Manufactured Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 70000
Est Cost Other 338521
Est Cost Other Details Osro; Other Costs Associated With Clean Up (Roll Off Boxes, Vacuum Boxes, Etc.)
Prpty 409021
Accident Psig 170
Mop Psig 590
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 27984
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release happened due to corrosion.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Other
Int Visual Exam Details Pin Hole
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details 0600 Orientation
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2016
Hydrtst Most Rcnt Pressure 761
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name Y******* B**
Preparer Title Pipeline Compliance Engineer
Preparer Email Y***@e****.com
Preparer Telephone 713-9068726
Prepared Date 2020-08-04 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 281-684-8179
Authorizer Title Pipeline Compliance Engineer
Authorizer Email D*******@e****.com
Narrative On 04/24/20 at 11:40, enterprise technician during station rounds discovered crude leaking on the ground from the bottom side of oth1 pipeline at the south manifold. The pipeline was isolated and a plidco clamp was installed. The pipeline was restored to its predefined level of service. Approximately 40 barrels was released inside the dike wall containment area. To prevent recurrence, this segment will be placed into quarterly dead leg flush program. All soil was remediated. Initial nrc call was made april 24, 2020 at 13:12 nrc# 1276009. The 48 hour update was placed april 26 at 10:56 nrc #1276115. Trrc was notified on 04/24/2020 at 12:11, incident # 2192.

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