HL incident on 2020-04-19 — TX

Operator
Glass Mountain Pipeline, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-04-19 09:54
Report number
Location
TX
Narrative
At approximately 9:54 am on april 19, 2020 the measurement technician discovered a crude oil release at the gmpl facility, omega station. The measurement technician shut in the valve and began initial emergency response activities. The release was contained within the gmpl facility. Notifications were made to the measurement technician's immediate supervisor, operations manager, ehs manager and vp of operations as per our emergency response plan. Occ notification was made via phone at 10:25 am. Acme environmental was contracted for environmental surface remediation. The packing on the external lever arm was leaking, thus found to be contributing factor of leaking equipment. Based on the investigation made during repairs it was found that check valve was altered from original design by previous operator. The valve was originally designed to be a non-swing arm valve but was altered to be a swing arm valve by blowing a hold thru the valve, welding a 2 inch nipple and attaching a swing arm. The valve could not be repaired and was replaced with the correct equipment. The operator has decided to go with internal flapper valve and eliminate the bushing as a potential failure point.
Detailed record list
Report Received Date
2020-05-18 00:00:00
Iyear
2020
Report Number
20200142
Supplemental Number
33994
Report Type
Supplemental Final
Operator Id
Name
Glass Mountain Pipeline, Llc
Operator Street Address
3625 N. Hall Street Suite 630
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2020-04-19 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-04-19 09:54:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-04-19 10:00:00
Restart Datetime
2020-04-20 00:00:00
On Site Datetime
2020-04-19 10:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Omega Station
Segment Name
Omega Station
Onshore State Abbreviation
Ok
Onshore Postal Code
73764
Onshore City Name
Omega
Onshore County Name
Blaine
Designated Location
Milepost/valve Station
Designated Name
Omega Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Design Issue
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
0
Est Cost Emergency
200
Est Cost Environmental
12959
Est Cost Other
0
Prpty
13189
Accident Psig
180
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controllers actions did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Bushing On External Lever Arm Was Leaking. Changed Internal Flapper Valve
Preparer Name
V****** R*****
Preparer Title
Ehs Regulatory Manager
Preparer Email
V******@n***********.com
Preparer Telephone
4327700179
Prepared Date
2020-07-02 00:00:00
Authorizer Name
V****** R*****
Authorizer Telephone
4327700179
Authorizer Title
Ehs Regulatory Manager
Authorizer Email
V******@n***********.com
Narrative
At approximately 9:54 am on april 19, 2020 the measurement technician discovered a crude oil release at the gmpl facility, omega station. The measurement technician shut in the valve and began initial emergency response activities. The release was contained within the gmpl facility. Notifications were made to the measurement technician's immediate supervisor, operations manager, ehs manager and vp of operations as per our emergency response plan. Occ notification was made via phone at 10:25 am. Acme environmental was contracted for environmental surface remediation. The packing on the external lever arm was leaking, thus found to be contributing factor of leaking equipment. Based on the investigation made during repairs it was found that check valve was altered from original design by previous operator. The valve was originally designed to be a non-swing arm valve but was altered to be a swing arm valve by blowing a hold thru the valve, welding a 2 inch nipple and attaching a swing arm. The valve could not be repaired and was replaced with the correct equipment. The operator has decided to go with internal flapper valve and eliminate the bushing as a potential failure point.
Report Received Date 2020-05-18 00:00:00
Iyear 2020
Report Number 20200142
Supplemental Number 33994
Report Type Supplemental Final
Operator Id 39774 PHMSA Enforcement
Name Glass Mountain Pipeline, Llc
Operator Street Address 3625 N. Hall Street Suite 630
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2020-04-19 10:00:00
Location Latitude 35.8435 Google Maps OpenStreetMap
Location Longitude -98.2496 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-04-19 09:54:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-04-19 10:00:00
Restart Datetime 2020-04-20 00:00:00
On Site Datetime 2020-04-19 10:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Omega Station
Segment Name Omega Station
Onshore State Abbreviation Ok
Onshore Postal Code 73764
Onshore City Name Omega
Onshore County Name Blaine
Designated Location Milepost/valve Station
Designated Name Omega Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Design Issue
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 0
Est Cost Emergency 200
Est Cost Environmental 12959
Est Cost Other 0
Prpty 13189
Accident Psig 180
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controllers actions did not contribute to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Bushing On External Lever Arm Was Leaking. Changed Internal Flapper Valve
Preparer Name V****** R*****
Preparer Title Ehs Regulatory Manager
Preparer Email V******@n***********.com
Preparer Telephone 4327700179
Prepared Date 2020-07-02 00:00:00
Authorizer Name V****** R*****
Authorizer Telephone 4327700179
Authorizer Title Ehs Regulatory Manager
Authorizer Email V******@n***********.com
Narrative At approximately 9:54 am on april 19, 2020 the measurement technician discovered a crude oil release at the gmpl facility, omega station. The measurement technician shut in the valve and began initial emergency response activities. The release was contained within the gmpl facility. Notifications were made to the measurement technician's immediate supervisor, operations manager, ehs manager and vp of operations as per our emergency response plan. Occ notification was made via phone at 10:25 am. Acme environmental was contracted for environmental surface remediation. The packing on the external lever arm was leaking, thus found to be contributing factor of leaking equipment. Based on the investigation made during repairs it was found that check valve was altered from original design by previous operator. The valve was originally designed to be a non-swing arm valve but was altered to be a swing arm valve by blowing a hold thru the valve, welding a 2 inch nipple and attaching a swing arm. The valve could not be repaired and was replaced with the correct equipment. The operator has decided to go with internal flapper valve and eliminate the bushing as a potential failure point.

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