GTG incident on 2020-12-04 — TX

Operator
Kinder Morgan Tejas Pipeline
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$110,536
Incident datetime
2020-12-04 16:40
Report number
Location
TX
Narrative
On december 4, 2020 at approximately 15:00 hrs. Local time, tejas pipeline received a call from a local gas operating company of natural gas vapors observed from a pipeline casing vent located near avery point in nueces county, texas. At 15:20 hrs. Local time, a tejas field technician inspected the location but could not locate the leak. The local gas operating company, originally reporting the leak, revised the location description to navigation blvd in nueces county, texas. Upon arrival at navigation blvd., the tejas field technician confirmed the leak belonged to tejas at 16:20 hrs. Local time by observing a low-level emission of vapors from the pipeline casing vent. The tejas field technician and management completed a erl telephone call and decided to report the event as an incident since it was determined that the cost of repairs would exceed $50,000. As such, tejas completed the report to the nrc at 17:02 hrs. The same day. Tejas completed a 48-hour nrc update the following day citing no significant changes. The pipe section containing the pinhole leak was shipped to bryan laboratories in houston, tx for metallurgical evaluation. Based on metallurgical report, the apparent cause of the pinhole leak appeared to be stray current induced on the pipeline from close proximity existing metal, narrow-gauge railroad line that crosses the tejas pipeline. The root cause of the pinhole leak was determined to be dc stray current from the railroad lines causing external corrosion of the pipeline directly below the tracks. The railroad tracks have been removed and the pipeline repaired and placed back into service. The affected pipe segment did not contain an injurious microstructure or properties that could have contribute to the failure. In addition, no internal corrosion reported.
Detailed record list
Report Received Date
2020-12-28 00:00:00
Iyear
2020
Report Number
20200134
Supplemental Number
35049
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Tejas Pipeline
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-12-04 17:02:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2020-12-04 17:02:00
Additional Nrc Report Numbers
1293611
Commodity Released Type
Natural Gas
Unintentional Release
104
Intentional Release
642
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-12-04 18:52:00
Still Shutdown Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2020-12-04 18:52:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2020-12-04 18:52:00
Num Pub Evacuated
0
Incident Identified Datetime
2020-12-04 16:40:00
On Site Datetime
2020-12-04 18:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78407
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Survey Station No.
Designated Name
21853.85
Pipe Fac Name
Transco To Avery
Segment Name
Goldston To Avery 12 Inch
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Underground Pipeline Casing.
Depth Of Cover
46
Other Underground Facilities
No
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Cased
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Puddle Weld Ind
No
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Fbe
Coating Applied Ind
Unknown
Installation Year
1988
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
252
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
281
Est Cost Intentional Release
1733
Est Cost Prop Damage
110536
Est Cost Emergency
500
Est Cost Other
0
Gas Cost In Mcf
2.7
Prpty
113050
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
669
Gas Flow In Pipe In Mcf
40000
Mop Psig
819
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1988-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
16913
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident was deemed independent of controller action.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Stray Current Type
Direct Current
Stray Current Details
Dc Current From Narrow Railroad Track Located Directly Above The Pipeline.
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1989
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2019
Close Interval Survey Year
2020
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2017
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Geometry Recent Year
2017
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Other Tool
Imu
Other Recent Year
2017
Other Rcnt Propul Method
Free Swimming
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** R* D****
Preparer Title
Engineer
Preparer Email
S************@k***********.com
Preparer Telephone
(719) 351-3199
Local Contact Name
T*** P*******
Local Contact Email
T************@k***********.com
Local Contact Telephone
(361) 438-3411
Authorizer Name
J**** H********
Authorizer Title
Director-Engineering
Authorizer Telephone
713 369-9443
Authorizer Email
J**************@k***********.com
Narrative
On december 4, 2020 at approximately 15:00 hrs. Local time, tejas pipeline received a call from a local gas operating company of natural gas vapors observed from a pipeline casing vent located near avery point in nueces county, texas. At 15:20 hrs. Local time, a tejas field technician inspected the location but could not locate the leak. The local gas operating company, originally reporting the leak, revised the location description to navigation blvd in nueces county, texas. Upon arrival at navigation blvd., the tejas field technician confirmed the leak belonged to tejas at 16:20 hrs. Local time by observing a low-level emission of vapors from the pipeline casing vent. The tejas field technician and management completed a erl telephone call and decided to report the event as an incident since it was determined that the cost of repairs would exceed $50,000. As such, tejas completed the report to the nrc at 17:02 hrs. The same day. Tejas completed a 48-hour nrc update the following day citing no significant changes. The pipe section containing the pinhole leak was shipped to bryan laboratories in houston, tx for metallurgical evaluation. Based on metallurgical report, the apparent cause of the pinhole leak appeared to be stray current induced on the pipeline from close proximity existing metal, narrow-gauge railroad line that crosses the tejas pipeline. The root cause of the pinhole leak was determined to be dc stray current from the railroad lines causing external corrosion of the pipeline directly below the tracks. The railroad tracks have been removed and the pipeline repaired and placed back into service. The affected pipe segment did not contain an injurious microstructure or properties that could have contribute to the failure. In addition, no internal corrosion reported.
Report Received Date 2020-12-28 00:00:00
Iyear 2020
Report Number 20200134
Supplemental Number 35049
Report Type Supplemental Final
Operator Id 4900 PHMSA Enforcement
Name Kinder Morgan Tejas Pipeline
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-12-04 17:02:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 27.817108 Google Maps OpenStreetMap
Location Longitude -97.452814 Google Maps OpenStreetMap
Nrc Rpt Num 1293563 NRC Report How to search
Nrc Rpt Datetime 2020-12-04 17:02:00
Additional Nrc Report Numbers 1293611
Commodity Released Type Natural Gas
Unintentional Release 104
Intentional Release 642
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-12-04 18:52:00
Still Shutdown Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2020-12-04 18:52:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2020-12-04 18:52:00
Num Pub Evacuated 0
Incident Identified Datetime 2020-12-04 16:40:00
On Site Datetime 2020-12-04 18:00:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78407
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Survey Station No.
Designated Name 21853.85
Pipe Fac Name Transco To Avery
Segment Name Goldston To Avery 12 Inch
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Underground Pipeline Casing.
Depth Of Cover 46
Other Underground Facilities No
Crossing Yes
Road Crossing Ind Yes
Road Type Cased
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Puddle Weld Ind No
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Fbe
Coating Applied Ind Unknown
Installation Year 1988
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 252
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 281
Est Cost Intentional Release 1733
Est Cost Prop Damage 110536
Est Cost Emergency 500
Est Cost Other 0
Gas Cost In Mcf 2.7
Prpty 113050
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 669
Gas Flow In Pipe In Mcf 40000
Mop Psig 819
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1988-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 16913
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident was deemed independent of controller action.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Stray Current Type Direct Current
Stray Current Details Dc Current From Narrow Railroad Track Located Directly Above The Pipeline.
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1989
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2019
Close Interval Survey Year 2020
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2017
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Geometry Recent Year 2017
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Other Tool Imu
Other Recent Year 2017
Other Rcnt Propul Method Free Swimming
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S****** R* D****
Preparer Title Engineer
Preparer Email S************@k***********.com
Preparer Telephone (719) 351-3199
Local Contact Name T*** P*******
Local Contact Email T************@k***********.com
Local Contact Telephone (361) 438-3411
Authorizer Name J**** H********
Authorizer Title Director-Engineering
Authorizer Telephone 713 369-9443
Authorizer Email J**************@k***********.com
Narrative On december 4, 2020 at approximately 15:00 hrs. Local time, tejas pipeline received a call from a local gas operating company of natural gas vapors observed from a pipeline casing vent located near avery point in nueces county, texas. At 15:20 hrs. Local time, a tejas field technician inspected the location but could not locate the leak. The local gas operating company, originally reporting the leak, revised the location description to navigation blvd in nueces county, texas. Upon arrival at navigation blvd., the tejas field technician confirmed the leak belonged to tejas at 16:20 hrs. Local time by observing a low-level emission of vapors from the pipeline casing vent. The tejas field technician and management completed a erl telephone call and decided to report the event as an incident since it was determined that the cost of repairs would exceed $50,000. As such, tejas completed the report to the nrc at 17:02 hrs. The same day. Tejas completed a 48-hour nrc update the following day citing no significant changes. The pipe section containing the pinhole leak was shipped to bryan laboratories in houston, tx for metallurgical evaluation. Based on metallurgical report, the apparent cause of the pinhole leak appeared to be stray current induced on the pipeline from close proximity existing metal, narrow-gauge railroad line that crosses the tejas pipeline. The root cause of the pinhole leak was determined to be dc stray current from the railroad lines causing external corrosion of the pipeline directly below the tracks. The railroad tracks have been removed and the pipeline repaired and placed back into service. The affected pipe segment did not contain an injurious microstructure or properties that could have contribute to the failure. In addition, no internal corrosion reported.

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