GD incident on 2020-11-23 — OH

Operator
Columbia Gas Of Ohio Inc
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$28,524
Incident datetime
2020-11-23 09:45
Report number
Location
OH, LAWRENCE
Narrative
On november 23, 2020, columbia was placing a repaired mainline in service and purging the line through a service line at the rear of a residential structure when an accidental ignition occurred. The ignition damaged the structure and four vehicles. During the purge, a grounded, 7' metallic purge stand was not utilized. Columbia evacuated the residential structure to ensure no residents were injured and shut down the mainline for safety. The individual purging the service line held the appropriate operator qualification for purging service lines but was not qualified to purge a mainline through a service line. The individual that was executing the purge was drug tested however an alcohol test was not conducted. Please consider this a final report.
Detailed record list
Occurred At
2020-11-23 09:45:00
Year
2020
Report Received Date
2020-12-23 00:00:00
Iyear
2020.0
Report Number
20200127.0
Supplemental Number
34952.0
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Of Ohio Inc
Operator Street Address
290 W Nationwide Blvd
Operator City Name
Columbus
Operator State Abbreviation
OH
Operator Postal Code
43215
Local Datetime
2020-11-23 09:45:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Street Address
3764 Cr15
Location City Name
South Point
Location County Name
Lawrence
Location State Abbreviation
OH
Location Postal Code
45680
Location Latitude
Location Longitude
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2020-11-23 21:51:00
Nrc Rpt Num
Additional Nrc Report Numbers
1292908
Commodity Released Type
Natural Gas
Unintentional Release
0.0
Intentional Release
1.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Ignite Datetime
2020-11-23 20:10:00
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
1
Explode Ind
No
Num Pub Evacuated
3.0
Incident Identified Datetime
2020-11-23 09:45:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2020-11-23 09:45:00
On Site Datetime
2020-11-23 09:45:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service Riser
Installation Year
2010.0
Customer Type
Single Family Residential
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
Yes
Material Involved
Other
Material Details
Meter Valve On Top Of Plastic Riser
Release Type
Other
Release Type Details
Purging Activity
Class Location Type
Class 3 Location
Est Cost Oper Paid
770000.0
Est Cost Prop Damage
28524.0
Est Cost Emergency
5900.0
Est Cost Other
0.0
Gas Cost In Mcf
2.0
Est Cost Unintentional Release
0.0
Est Cost Intentional Release
2.0
Prpty
804426.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
7.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
1.0
Num Resident Building Affctd
7.0
Num Business Building Affctd
0.0
Accident Psig
35.0
Normal Psig
35.0
Mop Psig
46.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
1970-01-23 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.5
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Failure To Prevent Accidental Ignition
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
Yes
Qualified Individuals
No, They Were Not Qualified For The Task(S) Nor Were They Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name
R** S****
Preparer Title
Manager Of Operations Compliance
Preparer Email
R******@n*******.com
Preparer Telephone
614-460-5491
Authorizer Name
R** S****
Authorizer Title
Manager Of Operations Compliance
Authorizer Telephone
614-460-5491
Authorizer Email
R******@n*******.com
Narrative
On november 23, 2020, columbia was placing a repaired mainline in service and purging the line through a service line at the rear of a residential structure when an accidental ignition occurred. The ignition damaged the structure and four vehicles. During the purge, a grounded, 7' metallic purge stand was not utilized. Columbia evacuated the residential structure to ensure no residents were injured and shut down the mainline for safety. The individual purging the service line held the appropriate operator qualification for purging service lines but was not qualified to purge a mainline through a service line. The individual that was executing the purge was drug tested however an alcohol test was not conducted. Please consider this a final report.
Occurred At 2020-11-23 09:45:00
Year 2020
Report Received Date 2020-12-23 00:00:00
Iyear 2020.0
Report Number 20200127.0
Supplemental Number 34952.0
Report Type Supplemental Final
Operator Id 2596 PHMSA Enforcement
Name Columbia Gas Of Ohio Inc
Operator Street Address 290 W Nationwide Blvd
Operator City Name Columbus
Operator State Abbreviation OH
Operator Postal Code 43215
Local Datetime 2020-11-23 09:45:00
Time Zone Eastern
Daylight Savings Ind No
Location Street Address 3764 Cr15
Location City Name South Point
Location County Name Lawrence
Location State Abbreviation OH
Location Postal Code 45680
Location Latitude 38.45443 Google Maps OpenStreetMap
Location Longitude -82.54555 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Datetime 2020-11-23 21:51:00
Nrc Rpt Num 1292897 NRC Report How to search
Additional Nrc Report Numbers 1292908
Commodity Released Type Natural Gas
Unintentional Release 0.0
Intentional Release 1.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Ignite Datetime 2020-11-23 20:10:00
How Extinguished Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf 1
Explode Ind No
Num Pub Evacuated 3.0
Incident Identified Datetime 2020-11-23 09:45:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2020-11-23 09:45:00
On Site Datetime 2020-11-23 09:45:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service Riser
Installation Year 2010.0
Customer Type Single Family Residential
Was Efv Installed Before Ind No
Curb Valve Inst Before Inc Ind Yes
Material Involved Other
Material Details Meter Valve On Top Of Plastic Riser
Release Type Other
Release Type Details Purging Activity
Class Location Type Class 3 Location
Est Cost Oper Paid 770000.0
Est Cost Prop Damage 28524.0
Est Cost Emergency 5900.0
Est Cost Other 0.0
Gas Cost In Mcf 2.0
Est Cost Unintentional Release 0.0
Est Cost Intentional Release 2.0
Prpty 804426.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 7.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 1.0
Num Resident Building Affctd 7.0
Num Business Building Affctd 0.0
Accident Psig 35.0
Normal Psig 35.0
Mop Psig 46.0
Mop Cfr Section 192.619(A)(3) View CFR 49 §192
Maop Established Date 1970-01-23 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 0.5
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Failure To Prevent Accidental Ignition
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind Yes
Qualified Individuals No, They Were Not Qualified For The Task(S) Nor Were They Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name R** S****
Preparer Title Manager Of Operations Compliance
Preparer Email R******@n*******.com
Preparer Telephone 614-460-5491
Authorizer Name R** S****
Authorizer Title Manager Of Operations Compliance
Authorizer Telephone 614-460-5491
Authorizer Email R******@n*******.com
Narrative On november 23, 2020, columbia was placing a repaired mainline in service and purging the line through a service line at the rear of a residential structure when an accidental ignition occurred. The ignition damaged the structure and four vehicles. During the purge, a grounded, 7' metallic purge stand was not utilized. Columbia evacuated the residential structure to ensure no residents were injured and shut down the mainline for safety. The individual purging the service line held the appropriate operator qualification for purging service lines but was not qualified to purge a mainline through a service line. The individual that was executing the purge was drug tested however an alcohol test was not conducted. Please consider this a final report.

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