GTG incident on 2020-10-18 — TX

Operator
Transwestern Pipeline Company Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-10-18 08:11
Report number
Location
TX
Narrative
08:11 mtn, october 18th technician contacted gas control to notify them of gas blowing. At 08:22 mtn isolated relief valve then tested and found that the relief control pilot would not hold a set point. Replaced with spare relief control pilot, retested and set pressure. 08:35 mtn, restarted units and found that everything was back to normal. 06:46 mtn, october 19th rough calculation of gas volume loss was completed, notified regulatory. 07:44 mtn, october 19th nrc notification was made nrc #1290106. 06:08 mtn, october 21st 48 hour nrc notification was made nrc #1290280, updated gas volume.
Detailed record list
Report Received Date
2020-11-17 00:00:00
Iyear
2020
Report Number
20200121
Supplemental Number
34543
Report Type
Original Final
Operator Id
Name
Transwestern Pipeline Company Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-10-19 06:02:00
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2020-10-19 07:44:00
Additional Nrc Report Numbers
1290280
Commodity Released Type
Natural Gas
Unintentional Release
7894
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-10-18 08:22:00
Restart Datetime
2020-10-18 08:35:00
Communication State Fed Ind
No
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2020-10-18 08:11:00
On Site Datetime
2020-10-18 08:15:00
On Off Shore
Onshore
Onshore State Abbreviation
Nm
Onshore Postal Code
88220
Onshore City Name
Carlsbad
Onshore County Name
Lea
Designated Location
Milepost
Designated Name
79.4
Pipe Fac Name
Wt-1 Carlsbad Compressor Station
Segment Name
Nmbw119
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
1960
Manufactured Year
1959
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Relief Valve Operation - Malfunction Of Relief Valve Due To Control Pilot.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
526
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
4736
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Other
0
Gas Cost In Mcf
0.6
Prpty
5236
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
988
Gas Flow In Pipe In Mcf
423
Mop Psig
1008
Mop Cfr Section
Maop Established Date
1960-01-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A relief valve failure was the cause of the gas release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Shorter Than Normal Life Of The Parts In The Pilot That Controls The Relief Valve.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Relief Valve Pilot Failure.
Preparer Name
K****** H*******
Preparer Email
K***************@e*************.com
Preparer Telephone
713-989-7085
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Email
T************@e*************.com
Narrative
08:11 mtn, october 18th technician contacted gas control to notify them of gas blowing. At 08:22 mtn isolated relief valve then tested and found that the relief control pilot would not hold a set point. Replaced with spare relief control pilot, retested and set pressure. 08:35 mtn, restarted units and found that everything was back to normal. 06:46 mtn, october 19th rough calculation of gas volume loss was completed, notified regulatory. 07:44 mtn, october 19th nrc notification was made nrc #1290106. 06:08 mtn, october 21st 48 hour nrc notification was made nrc #1290280, updated gas volume.
Report Received Date 2020-11-17 00:00:00
Iyear 2020
Report Number 20200121
Supplemental Number 34543
Report Type Original Final
Operator Id 19610 PHMSA Enforcement
Name Transwestern Pipeline Company Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-10-19 06:02:00
Time Zone Mountain
Daylight Savings Ind Yes
Location Latitude 32.532378 Google Maps OpenStreetMap
Location Longitude -103.809277 Google Maps OpenStreetMap
Nrc Rpt Num 1290106 NRC Report How to search
Nrc Rpt Datetime 2020-10-19 07:44:00
Additional Nrc Report Numbers 1290280
Commodity Released Type Natural Gas
Unintentional Release 7894
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-10-18 08:22:00
Restart Datetime 2020-10-18 08:35:00
Communication State Fed Ind No
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2020-10-18 08:11:00
On Site Datetime 2020-10-18 08:15:00
On Off Shore Onshore
Onshore State Abbreviation Nm
Onshore Postal Code 88220
Onshore City Name Carlsbad
Onshore County Name Lea
Designated Location Milepost
Designated Name 79.4
Pipe Fac Name Wt-1 Carlsbad Compressor Station
Segment Name Nmbw119
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Valve
Valve Type Relief Valve
Installation Year 1960
Manufactured Year 1959
Material Involved Carbon Steel
Release Type Other
Release Type Details Relief Valve Operation - Malfunction Of Relief Valve Due To Control Pilot.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 526
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 4736
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Other 0
Gas Cost In Mcf 0.6
Prpty 5236
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 988
Gas Flow In Pipe In Mcf 423
Mop Psig 1008
Mop Cfr Section 192.619(C) View CFR 49 §192
Maop Established Date 1960-01-01 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A relief valve failure was the cause of the gas release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Shorter Than Normal Life Of The Parts In The Pilot That Controls The Relief Valve.
Eq Additional Other Ind Yes
Eq Additional Other Details Relief Valve Pilot Failure.
Preparer Name K****** H*******
Preparer Email K***************@e*************.com
Preparer Telephone 713-989-7085
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Email T************@e*************.com
Narrative 08:11 mtn, october 18th technician contacted gas control to notify them of gas blowing. At 08:22 mtn isolated relief valve then tested and found that the relief control pilot would not hold a set point. Replaced with spare relief control pilot, retested and set pressure. 08:35 mtn, restarted units and found that everything was back to normal. 06:46 mtn, october 19th rough calculation of gas volume loss was completed, notified regulatory. 07:44 mtn, october 19th nrc notification was made nrc #1290106. 06:08 mtn, october 21st 48 hour nrc notification was made nrc #1290280, updated gas volume.

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