GTG incident on 2020-10-11 — TX

Operator
Stingray Pipeline Company, Llc
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-10-11 14:55
Report number
Location
TX
Narrative
The hi 330 platform was completely destroyed by hurricane delta on october 11th, 2020. The category 3 storm impacted the area with 125mph + winds and 10-25 ft waves. The 24" pipeline had been shutdown prior to the storm due to producers not having come back online yet from prior storms in the gulf. Upon inspection of the hi-330 platform on october 12th, 2020 and noting the 24" failure, the downstream valve was closed and the line isolated. A recovery plan is still being developed and evaluated. Supplemental report 11/12/2020 - clarification on a22: no actions taken upstream of failure. Et ownership begins at hi 330 and all upstream lines were severed due to hurricane damage. Only the downstream valve was shut in. - updated responses to e6, and e7. Supplemental/final report 05/03/2021 stingray pipeline company 24" pipeline remains isolated at this time and will be abandoned in place. Stingray pipeline does not have a firm timeline on removal of hi-a330 as that platform belongs to genesis.
Detailed record list
Report Received Date
2020-11-11 00:00:00
Iyear
2020
Report Number
20200120
Supplemental Number
36519
Report Type
Supplemental Final
Operator Id
Name
Stingray Pipeline Company, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-10-11 14:55:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-93.50274218
Nrc Rpt Num
Nrc Rpt Datetime
2020-10-12 11:51:00
Additional Nrc Report Numbers
1289549
Commodity Released Type
Natural Gas
Unintentional Release
63214
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Idle
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Pipeline Was Already In Idle Status And There Was No Flow From The Platform.
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2020-10-12 10:00:00
Num Pub Evacuated
0
Incident Identified Datetime
2020-10-11 14:55:00
On Site Datetime
2020-10-12 10:00:00
On Off Shore
Offshore
Pipe Fac Name
24" 100 Line
Segment Name
4813
Off Water Depth
255
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Ocs Type
Ocs-Gulf Of Mexico
Off Ocs Area
High Island
Off Ocs Block
330
Off Area Accident Type
Platform
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Puddle Weld Ind
No
Pipe Wall Thickness
0.5
Pipe Smys
60000
Pipe Specification
X60
Pipe Seam Type
Single Saw
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Concrete
Coating Applied Ind
Unknown
Installation Year
1977
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
75.4
Rupture Width
24
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
585
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
141599
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
100000
Est Cost Other Details
Estimated Costs Unknown Until Recovery Plan Is Fully Developed And Implemented.
Gas Cost In Mcf
2.24
Prpty
241599
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
720
Gas Flow In Pipe In Mcf
0
Mop Psig
1250
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1983-11-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Downstream Valve Type Ind
Manual
Length Segment Isolated
211147
Internal Inspection Ind
No
Diameter Change Ind
Yes
Unsuitable Mainline Ind
Yes
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Offshore Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Genesis Operator Of Platform Hi 330
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Natural environmental factors.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Other Natural Force Damage
Natural Force Type
Other Natural Force Damage
Nf Other Details
,,,,,,category 3 Hurricane Delta
Nf Extreme Weather Ind
Yes
Nf Hurricane Ind
Yes
Nf High Winds Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
7139897126
Authorizer Name
T*** N*******
Authorizer Title
Director - Regulatory Compliance
Authorizer Telephone
7139897126
Authorizer Email
T************@e*************.com
Narrative
The hi 330 platform was completely destroyed by hurricane delta on october 11th, 2020. The category 3 storm impacted the area with 125mph + winds and 10-25 ft waves. The 24" pipeline had been shutdown prior to the storm due to producers not having come back online yet from prior storms in the gulf. Upon inspection of the hi-330 platform on october 12th, 2020 and noting the 24" failure, the downstream valve was closed and the line isolated. A recovery plan is still being developed and evaluated. Supplemental report 11/12/2020 - clarification on a22: no actions taken upstream of failure. Et ownership begins at hi 330 and all upstream lines were severed due to hurricane damage. Only the downstream valve was shut in. - updated responses to e6, and e7. Supplemental/final report 05/03/2021 stingray pipeline company 24" pipeline remains isolated at this time and will be abandoned in place. Stingray pipeline does not have a firm timeline on removal of hi-a330 as that platform belongs to genesis.
Report Received Date 2020-11-11 00:00:00
Iyear 2020
Report Number 20200120
Supplemental Number 36519
Report Type Supplemental Final
Operator Id 40069 PHMSA Enforcement
Name Stingray Pipeline Company, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-10-11 14:55:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.0973385 Google Maps OpenStreetMap
Location Longitude -93.50274218 Google Maps OpenStreetMap
Nrc Rpt Num 1289546 NRC Report How to search
Nrc Rpt Datetime 2020-10-12 11:51:00
Additional Nrc Report Numbers 1289549
Commodity Released Type Natural Gas
Unintentional Release 63214
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Idle
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Pipeline Was Already In Idle Status And There Was No Flow From The Platform.
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2020-10-12 10:00:00
Num Pub Evacuated 0
Incident Identified Datetime 2020-10-11 14:55:00
On Site Datetime 2020-10-12 10:00:00
On Off Shore Offshore
Pipe Fac Name 24" 100 Line
Segment Name 4813
Off Water Depth 255
Off Accident Origin On The Outer Continental Shelf (Ocs)
Ocs Type Ocs-Gulf Of Mexico
Off Ocs Area High Island
Off Ocs Block 330
Off Area Accident Type Platform
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Puddle Weld Ind No
Pipe Wall Thickness 0.5
Pipe Smys 60000
Pipe Specification X60
Pipe Seam Type Single Saw
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Concrete
Coating Applied Ind Unknown
Installation Year 1977
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 75.4
Rupture Width 24
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 585
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 141599
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 100000
Est Cost Other Details Estimated Costs Unknown Until Recovery Plan Is Fully Developed And Implemented.
Gas Cost In Mcf 2.24
Prpty 241599
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 720
Gas Flow In Pipe In Mcf 0
Mop Psig 1250
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1983-11-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Downstream Valve Type Ind Manual
Length Segment Isolated 211147
Internal Inspection Ind No
Diameter Change Ind Yes
Unsuitable Mainline Ind Yes
Tight Mitered Ind Yes
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function Offshore Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Genesis Operator Of Platform Hi 330
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Natural environmental factors.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Other Natural Force Damage
Natural Force Type Other Natural Force Damage
Nf Other Details ,,,,,,category 3 Hurricane Delta
Nf Extreme Weather Ind Yes
Nf Hurricane Ind Yes
Nf High Winds Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 7139897126
Authorizer Name T*** N*******
Authorizer Title Director - Regulatory Compliance
Authorizer Telephone 7139897126
Authorizer Email T************@e*************.com
Narrative The hi 330 platform was completely destroyed by hurricane delta on october 11th, 2020. The category 3 storm impacted the area with 125mph + winds and 10-25 ft waves. The 24" pipeline had been shutdown prior to the storm due to producers not having come back online yet from prior storms in the gulf. Upon inspection of the hi-330 platform on october 12th, 2020 and noting the 24" failure, the downstream valve was closed and the line isolated. A recovery plan is still being developed and evaluated. Supplemental report 11/12/2020 - clarification on a22: no actions taken upstream of failure. Et ownership begins at hi 330 and all upstream lines were severed due to hurricane damage. Only the downstream valve was shut in. - updated responses to e6, and e7. Supplemental/final report 05/03/2021 stingray pipeline company 24" pipeline remains isolated at this time and will be abandoned in place. Stingray pipeline does not have a firm timeline on removal of hi-a330 as that platform belongs to genesis.

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