GD incident on 2020-09-09 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$87,072
Incident datetime
2020-09-09 12:35
Report number
Location
TX, DALLAS
Narrative
On september 9, 2020, a third-party contractor using an auger to install streetlights at 3178 lavon dr. In garland, tx struck atmos energy's 6-inch distribution line. Line locates had been called in and lines were marked correctly. No customers were affected by the incident; cng trucks were dispatched to supply gas during repairs. The 6-inch main was squeezed off at 4:33 am on 9/10/2020, and repairs began. The pipeline was placed back in service at 7:00 pm on 9/11/2020. Incident reporting criteria was met at 09:56 on 9/18/20 after it was determined that the property damage exceeded $50,000, and it was reported to the nrc at 10:31 on 9/18/2020. 48 hour nrc report # 1287826
Detailed record list
Occurred At
2020-09-09 12:35:00
Year
2020
Report Received Date
2020-10-15 00:00:00
Iyear
2020.0
Report Number
20200098.0
Supplemental Number
34380.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2020-09-18 09:56:00
Location Street Address
3178 Lavon Drive
Location City Name
Garland
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75040
Location Latitude
Location Longitude
-96.62117925
Nrc Rpt Datetime
2020-09-18 10:31:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
435.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-09-09 12:35:00
On Site Datetime
2020-09-09 12:35:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
52.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2005.0
Pipe Diameter
6.0
Pipe Specification
Api 5l 45th Edition
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Erw
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
87072.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
2490.0
Prpty
89562.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
73.0
Normal Psig
75.0
Mop Psig
95.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
3rd party damage by contractor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Util Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Street Light
One Call Notified Ind
Yes
One Call Ticket Num
2074640492
One Call Center Name
Texas811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
E******** D******
Preparer Title
Operations Manager
Preparer Email
E****************@a**********.com
Preparer Telephone
972-485-6256
Preparer Fax
972-485-6267
Authorizer Name
M**** S*****
Authorizer Title
Vice President - Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
On september 9, 2020, a third-party contractor using an auger to install streetlights at 3178 lavon dr. In garland, tx struck atmos energy's 6-inch distribution line. Line locates had been called in and lines were marked correctly. No customers were affected by the incident; cng trucks were dispatched to supply gas during repairs. The 6-inch main was squeezed off at 4:33 am on 9/10/2020, and repairs began. The pipeline was placed back in service at 7:00 pm on 9/11/2020. Incident reporting criteria was met at 09:56 on 9/18/20 after it was determined that the property damage exceeded $50,000, and it was reported to the nrc at 10:31 on 9/18/2020. 48 hour nrc report # 1287826
Occurred At 2020-09-09 12:35:00
Year 2020
Report Received Date 2020-10-15 00:00:00
Iyear 2020.0
Report Number 20200098.0
Supplemental Number 34380.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2020-09-18 09:56:00
Location Street Address 3178 Lavon Drive
Location City Name Garland
Location County Name Dallas
Location State Abbreviation TX
Location Postal Code 75040
Location Latitude 32.94559754 Google Maps OpenStreetMap
Location Longitude -96.62117925 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-09-18 10:31:00
Nrc Rpt Num 1287688 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 435.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-09-09 12:35:00
On Site Datetime 2020-09-09 12:35:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 52.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2005.0
Pipe Diameter 6.0
Pipe Specification Api 5l 45th Edition
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Erw
Wt Steel 0.188
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 0.5
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 87072.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 2490.0
Prpty 89562.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 73.0
Normal Psig 75.0
Mop Psig 95.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details 3rd party damage by contractor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Util Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Street Light
One Call Notified Ind Yes
One Call Ticket Num 2074640492
One Call Center Name Texas811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption No
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name E******** D******
Preparer Title Operations Manager
Preparer Email E****************@a**********.com
Preparer Telephone 972-485-6256
Preparer Fax 972-485-6267
Authorizer Name M**** S*****
Authorizer Title Vice President - Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative On september 9, 2020, a third-party contractor using an auger to install streetlights at 3178 lavon dr. In garland, tx struck atmos energy's 6-inch distribution line. Line locates had been called in and lines were marked correctly. No customers were affected by the incident; cng trucks were dispatched to supply gas during repairs. The 6-inch main was squeezed off at 4:33 am on 9/10/2020, and repairs began. The pipeline was placed back in service at 7:00 pm on 9/11/2020. Incident reporting criteria was met at 09:56 on 9/18/20 after it was determined that the property damage exceeded $50,000, and it was reported to the nrc at 10:31 on 9/18/2020. 48 hour nrc report # 1287826

All rights reserved. Copyright © by ClearPHMSA