GD incident on 2020-09-02 — NE

Operator
Black Hills Energy
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$190,000
Incident datetime
2020-09-02 11:30
Report number
Location
NE, LANCASTER
Narrative
Gas leak was called in to this location by customer smelling gas outside for 3 minutes on sept 2, 2020. Bhe technician responded performed outside leak investigation. Lz-30 and cgi instruments detected underground leak and was pinpointed under the concrete of o street. O street traffic was closed and concrete was removed to ventilate leak. Leak was on 16 inch steel main and later determined to be a pinhole corrosion leak. A 16 inch short stop needed to be ordered and contractor hired to install stop in order to do repair. Street remained closed to allow venting of pinhole leak until 9-12-2020 as date of repair. To repair leak, an existing short stop was used along with a newly installed shortstop to isolate the leak and cut out pipe section to replace. The corrosion department investigated this determined that the steel main was poorly coated 1931 vintage pipe and the point of corrosion was directly under poor coating. It had a corrosion rate of 2.8 mpy. Cp test points close to this location had sufficient cp protection historically, but were not sufficient in the bell hole of where the leak occurred. Bhe installed 6 anodes in the bell hole of the main at this location to raise cp protection to an acceptable level. Cp test points remain at an acceptable level of protection after repair. On 9-16-2020, it was determined that costs of equipment, contractors, and street repair exceeded the $50,000 level of reporting.
Detailed record list
Occurred At
2020-09-02 11:30:00
Year
2020
Report Received Date
2020-10-15 00:00:00
Iyear
2020.0
Report Number
20200097.0
Supplemental Number
34680.0
Report Type
Supplemental Final
Operator Id
Name
Black Hills Energy
Operator Street Address
2287 College Road Po Box 2006
Operator City Name
Council Bluffs
Operator State Abbreviation
IA
Operator Postal Code
51502
Local Datetime
2020-09-02 10:34:00
Time Zone
Central
Daylight Savings Ind
No
Location Street Address
3401 O Street
Location City Name
Lincoln
Location County Name
Lancaster
Location State Abbreviation
NE
Location Postal Code
68510
Location Latitude
Location Longitude
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2020-09-16 14:42:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
2.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-09-02 11:30:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2020-09-02 10:45:00
On Site Datetime
2020-09-02 11:24:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
24.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1931.0
Pipe Diameter
16.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.25
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 3 Location
Est Cost Oper Paid
60000.0
Est Cost Prop Damage
190000.0
Est Cost Emergency
50000.0
Est Cost Other
15000.0
Est Cost Other Details
Traffic Control, Ems
Gas Cost In Mcf
20.0
Est Cost Unintentional Release
40.0
Est Cost Intentional Release
0.0
Prpty
315040.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
2.0
Accident Psig
70.0
Normal Psig
70.0
Mop Psig
74.0
Mop Cfr Section
192.619(A)(4)
Maop Established Date
1994-02-23 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.1
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Poorly Coated 1931 Vintage Pipe With Bad Coating At Point Of Corrosion Failure.
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2020
Other Cp Survey Year
2020
Other Cp Survey Details
Cp Surveys In Area Immediately After Incident Were Compliant
Prior Damage
Yes
Coating Type
Other
Coating Type Details
Field Applied Mop/hand Coaltar
Field Applied Ind
Yes
Cor Hydrotest Leak Survey Date
2018-08-08 00:00:00
Cor Hydrotest Conducted Ind
No
Preparer Name
T** D********
Preparer Title
Pipeline Safety Compliance Coordinator
Preparer Email
T************@b*************.com
Preparer Telephone
308 760 4592
Authorizer Name
T** D********
Authorizer Title
Pipeline Safety Compliance Coordinator
Authorizer Telephone
402 858 3602
Authorizer Email
T************@b*************.com
Narrative
Gas leak was called in to this location by customer smelling gas outside for 3 minutes on sept 2, 2020. Bhe technician responded performed outside leak investigation. Lz-30 and cgi instruments detected underground leak and was pinpointed under the concrete of o street. O street traffic was closed and concrete was removed to ventilate leak. Leak was on 16 inch steel main and later determined to be a pinhole corrosion leak. A 16 inch short stop needed to be ordered and contractor hired to install stop in order to do repair. Street remained closed to allow venting of pinhole leak until 9-12-2020 as date of repair. To repair leak, an existing short stop was used along with a newly installed shortstop to isolate the leak and cut out pipe section to replace. The corrosion department investigated this determined that the steel main was poorly coated 1931 vintage pipe and the point of corrosion was directly under poor coating. It had a corrosion rate of 2.8 mpy. Cp test points close to this location had sufficient cp protection historically, but were not sufficient in the bell hole of where the leak occurred. Bhe installed 6 anodes in the bell hole of the main at this location to raise cp protection to an acceptable level. Cp test points remain at an acceptable level of protection after repair. On 9-16-2020, it was determined that costs of equipment, contractors, and street repair exceeded the $50,000 level of reporting.
Occurred At 2020-09-02 11:30:00
Year 2020
Report Received Date 2020-10-15 00:00:00
Iyear 2020.0
Report Number 20200097.0
Supplemental Number 34680.0
Report Type Supplemental Final
Operator Id 15359 PHMSA Enforcement
Name Black Hills Energy
Operator Street Address 2287 College Road Po Box 2006
Operator City Name Council Bluffs
Operator State Abbreviation IA
Operator Postal Code 51502
Local Datetime 2020-09-02 10:34:00
Time Zone Central
Daylight Savings Ind No
Location Street Address 3401 O Street
Location City Name Lincoln
Location County Name Lancaster
Location State Abbreviation NE
Location Postal Code 68510
Location Latitude 40.813258 Google Maps OpenStreetMap
Location Longitude -96.671531 Google Maps OpenStreetMap
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2020-09-16 14:42:00
Nrc Rpt Num 1287516 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 2.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-09-02 11:30:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2020-09-02 10:45:00
On Site Datetime 2020-09-02 11:24:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 24.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1931.0
Pipe Diameter 16.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.25
Release Type Leak
Leak Type Pinhole
Class Location Type Class 3 Location
Est Cost Oper Paid 60000.0
Est Cost Prop Damage 190000.0
Est Cost Emergency 50000.0
Est Cost Other 15000.0
Est Cost Other Details Traffic Control, Ems
Gas Cost In Mcf 20.0
Est Cost Unintentional Release 40.0
Est Cost Intentional Release 0.0
Prpty 315040.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 2.0
Accident Psig 70.0
Normal Psig 70.0
Mop Psig 74.0
Mop Cfr Section 192.619(A)(4) View CFR 49 §192
Maop Established Date 1994-02-23 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 0.1
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Poorly Coated 1931 Vintage Pipe With Bad Coating At Point Of Corrosion Failure.
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2020
Other Cp Survey Year 2020
Other Cp Survey Details Cp Surveys In Area Immediately After Incident Were Compliant
Prior Damage Yes
Coating Type Other
Coating Type Details Field Applied Mop/hand Coaltar
Field Applied Ind Yes
Cor Hydrotest Leak Survey Date 2018-08-08 00:00:00
Cor Hydrotest Conducted Ind No
Preparer Name T** D********
Preparer Title Pipeline Safety Compliance Coordinator
Preparer Email T************@b*************.com
Preparer Telephone 308 760 4592
Authorizer Name T** D********
Authorizer Title Pipeline Safety Compliance Coordinator
Authorizer Telephone 402 858 3602
Authorizer Email T************@b*************.com
Narrative Gas leak was called in to this location by customer smelling gas outside for 3 minutes on sept 2, 2020. Bhe technician responded performed outside leak investigation. Lz-30 and cgi instruments detected underground leak and was pinpointed under the concrete of o street. O street traffic was closed and concrete was removed to ventilate leak. Leak was on 16 inch steel main and later determined to be a pinhole corrosion leak. A 16 inch short stop needed to be ordered and contractor hired to install stop in order to do repair. Street remained closed to allow venting of pinhole leak until 9-12-2020 as date of repair. To repair leak, an existing short stop was used along with a newly installed shortstop to isolate the leak and cut out pipe section to replace. The corrosion department investigated this determined that the steel main was poorly coated 1931 vintage pipe and the point of corrosion was directly under poor coating. It had a corrosion rate of 2.8 mpy. Cp test points close to this location had sufficient cp protection historically, but were not sufficient in the bell hole of where the leak occurred. Bhe installed 6 anodes in the bell hole of the main at this location to raise cp protection to an acceptable level. Cp test points remain at an acceptable level of protection after repair. On 9-16-2020, it was determined that costs of equipment, contractors, and street repair exceeded the $50,000 level of reporting.

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