GTG incident on 2020-05-19 — TX

Operator
Anr Pipeline Co
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$400,000
Incident datetime
2020-05-19 12:46
Report number
Location
TX
Narrative
A root cause failure analysis (rcfa) final report, which incorporated the findings from the mechanical and metallurgical testing report summarized the event as, "... A rupture of facility piping on the shell side of the gas-gas heat exchanger (e-2053) leading to the ejection of process piping as well as the release of natural gas to the environment. Causal factors were recognized for the event sequences pertaining to (1) a natural gas leak from the high pressure injection header to lower pressure process piping through isolation valve xv-2070 and xv-2071 and (2) inadequate safety systems in the shell side of the heat exchanger loop to prevent rupture of the lower maop piping." metallurgical lab completed the failure analysis of the fractured piping and concluded that the rupture of the shell side piping was caused by ductile overload from pipe over-pressurization. Causal factors were identified as: leaking isolation valves; inadequate design-no overpressure protection or alarms; no positive isolation of shell side loop. Based on the rcfa, recommendations and potential improvement opportunities identified, corrective actions have been assigned to address each contributing factor.
Detailed record list
Report Received Date
2020-06-19 00:00:00
Iyear
2020
Report Number
20200065
Supplemental Number
34502
Report Type
Supplemental Final
Operator Id
Name
Anr Pipeline Co
Operator Street Address
700 Louisiana Street Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-05-19 12:46:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2020-05-19 14:33:00
Additional Nrc Report Numbers
1277764
Commodity Released Type
Natural Gas
Unintentional Release
26.5
Intentional Release
2156
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-05-19 13:20:00
Still Shutdown Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Initial Responder Com Datetime
2020-05-19 13:50:00
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2020-05-19 12:46:00
On Site Datetime
2020-05-19 13:19:00
On Off Shore
Onshore
Onshore State Abbreviation
Mi
Onshore Postal Code
49646
Onshore City Name
Excelsior Township
Onshore County Name
Kalkaska
Designated Location
Not Applicable
Pipe Fac Name
Excelsior 6 Compressor Station
Segment Name
Anr Storage
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
20
Pipe Wall Thickness
0.375
Pipe Smys
60000
Pipe Specification
Api-5l Pls2 X60
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Salzgitter Mannesmann Line Pipe
Pipe Coating Type
Paint
Coating Applied Ind
Yes
Installation Year
2018
Manufactured Year
2017
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
62.8
Rupture Width
62.8
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
467
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
46
Est Cost Intentional Release
3751
Est Cost Prop Damage
400000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
1.74
Prpty
403797
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
2961
Gas Flow In Pipe In Mcf
0
Mop Psig
1050
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2018-09-22 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Exceeded The Applicable Allowance In 192.201
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Pipeline Function
Transmission In Storage Field
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Additional Overpressure Ind
Yes
Preparer Name
R****** P******
Preparer Title
Compliance Specialist
Preparer Email
R**************@t*******.com
Preparer Telephone
248-561-7803
Authorizer Name
L** R*****
Authorizer Title
Director Pipeline Regulator Compliance
Authorizer Telephone
832-320-5315
Authorizer Email
L*********@t*******.com
Narrative
A root cause failure analysis (rcfa) final report, which incorporated the findings from the mechanical and metallurgical testing report summarized the event as, "... A rupture of facility piping on the shell side of the gas-gas heat exchanger (e-2053) leading to the ejection of process piping as well as the release of natural gas to the environment. Causal factors were recognized for the event sequences pertaining to (1) a natural gas leak from the high pressure injection header to lower pressure process piping through isolation valve xv-2070 and xv-2071 and (2) inadequate safety systems in the shell side of the heat exchanger loop to prevent rupture of the lower maop piping." metallurgical lab completed the failure analysis of the fractured piping and concluded that the rupture of the shell side piping was caused by ductile overload from pipe over-pressurization. Causal factors were identified as: leaking isolation valves; inadequate design-no overpressure protection or alarms; no positive isolation of shell side loop. Based on the rcfa, recommendations and potential improvement opportunities identified, corrective actions have been assigned to address each contributing factor.
Report Received Date 2020-06-19 00:00:00
Iyear 2020
Report Number 20200065
Supplemental Number 34502
Report Type Supplemental Final
Operator Id 405 PHMSA Enforcement
Name Anr Pipeline Co
Operator Street Address 700 Louisiana Street Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-05-19 12:46:00
Time Zone Eastern
Daylight Savings Ind No
Location Latitude 44.77025 Google Maps OpenStreetMap
Location Longitude -85.07459 Google Maps OpenStreetMap
Nrc Rpt Num 1277651 NRC Report How to search
Nrc Rpt Datetime 2020-05-19 14:33:00
Additional Nrc Report Numbers 1277764
Commodity Released Type Natural Gas
Unintentional Release 26.5
Intentional Release 2156
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-05-19 13:20:00
Still Shutdown Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Initial Responder Com Datetime 2020-05-19 13:50:00
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2020-05-19 12:46:00
On Site Datetime 2020-05-19 13:19:00
On Off Shore Onshore
Onshore State Abbreviation Mi
Onshore Postal Code 49646
Onshore City Name Excelsior Township
Onshore County Name Kalkaska
Designated Location Not Applicable
Pipe Fac Name Excelsior 6 Compressor Station
Segment Name Anr Storage
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 20
Pipe Wall Thickness 0.375
Pipe Smys 60000
Pipe Specification Api-5l Pls2 X60
Pipe Seam Type Longitudinal Erw - High Frequency
Pipe Manufacturer Salzgitter Mannesmann Line Pipe
Pipe Coating Type Paint
Coating Applied Ind Yes
Installation Year 2018
Manufactured Year 2017
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 62.8
Rupture Width 62.8
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 467
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 46
Est Cost Intentional Release 3751
Est Cost Prop Damage 400000
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 1.74
Prpty 403797
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 2961
Gas Flow In Pipe In Mcf 0
Mop Psig 1050
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2018-09-22 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Exceeded The Applicable Allowance In 192.201
Pressure Restriction Ind No
Gas Required Odorized Ind No
Pipeline Function Transmission In Storage Field
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Additional Overpressure Ind Yes
Preparer Name R****** P******
Preparer Title Compliance Specialist
Preparer Email R**************@t*******.com
Preparer Telephone 248-561-7803
Authorizer Name L** R*****
Authorizer Title Director Pipeline Regulator Compliance
Authorizer Telephone 832-320-5315
Authorizer Email L*********@t*******.com
Narrative A root cause failure analysis (rcfa) final report, which incorporated the findings from the mechanical and metallurgical testing report summarized the event as, "... A rupture of facility piping on the shell side of the gas-gas heat exchanger (e-2053) leading to the ejection of process piping as well as the release of natural gas to the environment. Causal factors were recognized for the event sequences pertaining to (1) a natural gas leak from the high pressure injection header to lower pressure process piping through isolation valve xv-2070 and xv-2071 and (2) inadequate safety systems in the shell side of the heat exchanger loop to prevent rupture of the lower maop piping." metallurgical lab completed the failure analysis of the fractured piping and concluded that the rupture of the shell side piping was caused by ductile overload from pipe over-pressurization. Causal factors were identified as: leaking isolation valves; inadequate design-no overpressure protection or alarms; no positive isolation of shell side loop. Based on the rcfa, recommendations and potential improvement opportunities identified, corrective actions have been assigned to address each contributing factor.

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