GD incident on 2020-05-08 — MN

Operator
Northern States Power Co Of Minnesota
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500,000
Incident datetime
2020-05-08 15:13
Report number
Location
MN, WASHINGTON
Narrative
On may 8, 2020, northern states power company, minnesota (nspm) was notified regarding a blowing gas situation. The investigation revealed that an abandoned six inch steel, coal tar coating pipeline was located. An existing 12 inch steel fbe coated high pressure distribution line was not located. Review of the bore profile determined the 12 inch main that was installed in 2018 was approximately 25 feet at the point of damage. Nspm attempted to excavate the main at the point of damaged and later determined due to depth, it was safer to not expose the main at the point of damage and install approximately 1100 feet of new 12 inch steel. Estimated gas loss was calculated from scada data at the time of the damage. Point of damage was not exposed so size of puncture is not known for part d: question 2.D review of existing damage prevention processes was conducted and found that the individual responsible for verifying the size and type of pipe that was exposed did not follow those processes.
Detailed record list
Occurred At
2020-05-08 15:13:00
Year
2020
Report Received Date
2020-06-11 00:00:00
Iyear
2020.0
Report Number
20200056.0
Supplemental Number
34317.0
Report Type
Supplemental Final
Operator Id
Name
Northern States Power Co Of Minnesota
Operator Street Address
414 Nicollet Mall
Operator City Name
Minneapolis
Operator State Abbreviation
MN
Operator Postal Code
55402
Local Datetime
2020-05-11 17:00:00
Location Street Address
Valley Creek Drive And Tower Drive
Location City Name
Woodbury
Location County Name
Washington
Location State Abbreviation
MN
Location Postal Code
55125
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-05-11 17:00:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1405.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-05-08 15:13:00
On Site Datetime
2020-05-08 15:25:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
300.0
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Bored/drilled
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2018.0
Pipe Diameter
12.0
Pipe Specification
Api 5l
Pipe Manufacturer
Tenaris
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - High Frequency
Steel Seam Type Details
High Frequency Weld
Wt Steel
0.375
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
50000.0
Est Cost Prop Damage
1500000.0
Est Cost Emergency
3737.0
Est Cost Other
0.0
Est Cost Unintentional Release
3204.0
Prpty
1556941.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
196.0
Normal Psig
200.0
Mop Psig
220.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was caused by 3rd party excavator
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Excavator Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
County Road
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
201135196
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Unlocatable Facility
Preparer Name
L*** K*******
Preparer Title
Principal Consultant Gas Standards
Preparer Email
E*******************@x*********.com
Preparer Telephone
651-229-2282
Authorizer Name
C********** A****
Authorizer Title
Manager Gas Standards
Authorizer Telephone
303-571-3298
Authorizer Email
C******************@x*********.com
Narrative
On may 8, 2020, northern states power company, minnesota (nspm) was notified regarding a blowing gas situation. The investigation revealed that an abandoned six inch steel, coal tar coating pipeline was located. An existing 12 inch steel fbe coated high pressure distribution line was not located. Review of the bore profile determined the 12 inch main that was installed in 2018 was approximately 25 feet at the point of damage. Nspm attempted to excavate the main at the point of damaged and later determined due to depth, it was safer to not expose the main at the point of damage and install approximately 1100 feet of new 12 inch steel. Estimated gas loss was calculated from scada data at the time of the damage. Point of damage was not exposed so size of puncture is not known for part d: question 2.D review of existing damage prevention processes was conducted and found that the individual responsible for verifying the size and type of pipe that was exposed did not follow those processes.
Occurred At 2020-05-08 15:13:00
Year 2020
Report Received Date 2020-06-11 00:00:00
Iyear 2020.0
Report Number 20200056.0
Supplemental Number 34317.0
Report Type Supplemental Final
Operator Id 31636 PHMSA Enforcement
Name Northern States Power Co Of Minnesota
Operator Street Address 414 Nicollet Mall
Operator City Name Minneapolis
Operator State Abbreviation MN
Operator Postal Code 55402
Local Datetime 2020-05-11 17:00:00
Location Street Address Valley Creek Drive And Tower Drive
Location City Name Woodbury
Location County Name Washington
Location State Abbreviation MN
Location Postal Code 55125
Location Latitude 44.920019 Google Maps OpenStreetMap
Location Longitude -92.944151 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-05-11 17:00:00
Nrc Rpt Num 1277068 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1405.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-05-08 15:13:00
On Site Datetime 2020-05-08 15:25:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 300.0
Crossing Yes
Road Crossing Ind Yes
Road Type Bored/drilled
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2018.0
Pipe Diameter 12.0
Pipe Specification Api 5l
Pipe Manufacturer Tenaris
Material Involved Steel
Steel Seam Type Longitudinal Erw - High Frequency
Steel Seam Type Details High Frequency Weld
Wt Steel 0.375
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 50000.0
Est Cost Prop Damage 1500000.0
Est Cost Emergency 3737.0
Est Cost Other 0.0
Est Cost Unintentional Release 3204.0
Prpty 1556941.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 196.0
Normal Psig 200.0
Mop Psig 220.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was caused by 3rd party excavator
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Excavator Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype County Road
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 201135196
Locator Type Contract Locator
Visible Marks No
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Unlocatable Facility
Preparer Name L*** K*******
Preparer Title Principal Consultant Gas Standards
Preparer Email E*******************@x*********.com
Preparer Telephone 651-229-2282
Authorizer Name C********** A****
Authorizer Title Manager Gas Standards
Authorizer Telephone 303-571-3298
Authorizer Email C******************@x*********.com
Narrative On may 8, 2020, northern states power company, minnesota (nspm) was notified regarding a blowing gas situation. The investigation revealed that an abandoned six inch steel, coal tar coating pipeline was located. An existing 12 inch steel fbe coated high pressure distribution line was not located. Review of the bore profile determined the 12 inch main that was installed in 2018 was approximately 25 feet at the point of damage. Nspm attempted to excavate the main at the point of damaged and later determined due to depth, it was safer to not expose the main at the point of damage and install approximately 1100 feet of new 12 inch steel. Estimated gas loss was calculated from scada data at the time of the damage. Point of damage was not exposed so size of puncture is not known for part d: question 2.D review of existing damage prevention processes was conducted and found that the individual responsible for verifying the size and type of pipe that was exposed did not follow those processes.

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