GD incident on 2020-05-05 — CA

Operator
Southern California Gas Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,540
Incident datetime
2020-05-05 10:50
Report number
Location
CA, TULARE
Narrative
On may 5, 2020, socalgas crew was working on a service abandonment job and damaged a 1-inch service tee with a backhoe. The service was fed from a 4-inch steel high pressure main. Gas was controlled by cold pinching the 4-inch high pressure steel main at two locations to the east and west of the damage. There were no injuries or further damage resulting from this incident. The 4-inch main was repaired by welding on pressure control fittings, stopping the main with pressure control equipment, cutting out the cold squeezes, and replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket and the 4-inch main was properly marked. Socalgas crew failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.
Detailed record list
Occurred At
2020-05-05 10:50:00
Year
2020
Report Received Date
2020-06-05 00:00:00
Iyear
2020.0
Report Number
20200054.0
Supplemental Number
33866.0
Report Type
Original Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2020-05-05 10:50:00
Location Street Address
13086 Avenue 384
Location City Name
Cutler
Location County Name
Tulare
Location State Abbreviation
CA
Location Postal Code
93615
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-05-07 17:57:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
503.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-05-05 10:50:00
On Site Datetime
2020-05-05 10:50:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1940.0
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.178
Release Type
Other
Release Type Details
0.500" Hole In 4" Main Due To Mechanical Damage.
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
10540.0
Est Cost Emergency
90708.0
Est Cost Other
0.0
Est Cost Unintentional Release
3018.0
Prpty
104266.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
170.0
Normal Psig
170.0
Mop Psig
175.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator (First Party)
Ex Party Type
Excavation Damage By Operator (First Party)
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Utility
Excavator Equipment
Backhoe/trackhoe
Work Performed
Natural Gas
One Call Notified Ind
Yes
One Call Ticket Num
X012200988
One Call Center Name
Usa North
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
A** M****
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
A*****@s*******.com
Preparer Telephone
909-919-0463
Authorizer Name
A** M****
Authorizer Title
Pipeline Safety And Compliance Advisor
Authorizer Telephone
909-919-0463
Authorizer Email
A*****@s*******.com
Narrative
On may 5, 2020, socalgas crew was working on a service abandonment job and damaged a 1-inch service tee with a backhoe. The service was fed from a 4-inch steel high pressure main. Gas was controlled by cold pinching the 4-inch high pressure steel main at two locations to the east and west of the damage. There were no injuries or further damage resulting from this incident. The 4-inch main was repaired by welding on pressure control fittings, stopping the main with pressure control equipment, cutting out the cold squeezes, and replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket and the 4-inch main was properly marked. Socalgas crew failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.
Occurred At 2020-05-05 10:50:00
Year 2020
Report Received Date 2020-06-05 00:00:00
Iyear 2020.0
Report Number 20200054.0
Supplemental Number 33866.0
Report Type Original Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2020-05-05 10:50:00
Location Street Address 13086 Avenue 384
Location City Name Cutler
Location County Name Tulare
Location State Abbreviation CA
Location Postal Code 93615
Location Latitude 36.4867 Google Maps OpenStreetMap
Location Longitude -119.2803 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-05-07 17:57:00
Nrc Rpt Num 1276850 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 503.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-05-05 10:50:00
On Site Datetime 2020-05-05 10:50:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 28.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1940.0
Pipe Diameter 4.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.178
Release Type Other
Release Type Details 0.500" Hole In 4" Main Due To Mechanical Damage.
Class Location Type Class 1 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 10540.0
Est Cost Emergency 90708.0
Est Cost Other 0.0
Est Cost Unintentional Release 3018.0
Prpty 104266.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 170.0
Normal Psig 170.0
Mop Psig 175.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Operator (First Party)
Ex Party Type Excavation Damage By Operator (First Party)
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype State Highway
Excavator Type Utility
Excavator Equipment Backhoe/trackhoe
Work Performed Natural Gas
One Call Notified Ind Yes
One Call Ticket Num X012200988
One Call Center Name Usa North
Locator Type Utility Owner
Visible Marks Yes
Service Interruption No
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name A** M****
Preparer Title Pipeline Safety And Compliance Advisor
Preparer Email A*****@s*******.com
Preparer Telephone 909-919-0463
Authorizer Name A** M****
Authorizer Title Pipeline Safety And Compliance Advisor
Authorizer Telephone 909-919-0463
Authorizer Email A*****@s*******.com
Narrative On may 5, 2020, socalgas crew was working on a service abandonment job and damaged a 1-inch service tee with a backhoe. The service was fed from a 4-inch steel high pressure main. Gas was controlled by cold pinching the 4-inch high pressure steel main at two locations to the east and west of the damage. There were no injuries or further damage resulting from this incident. The 4-inch main was repaired by welding on pressure control fittings, stopping the main with pressure control equipment, cutting out the cold squeezes, and replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket and the 4-inch main was properly marked. Socalgas crew failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.

All rights reserved. Copyright © by ClearPHMSA