GD incident on 2020-05-08 — CA

Operator
Southern California Gas Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2020-05-08 10:53
Report number
Location
CA, LOS ANGELES
Narrative
On may 8, 2020, a third-party contractor damaged a 6-inch steel gas main while boring to install conduit. Socalgas crews responded and controlled the gas with pressure control equipment. There were no injuries or further damage resulting from this incident. The 6-inch main was repaired by welding a wedding band. Investigation of the incident showed that there was a valid USA ticket, however, the 6-inch main was not marked out by the locator. Ticket had been left open in "project" status by the locator to return on a later date to complete. The locator did not address the ticket before the due date upon his return to work from his time off (7 days). This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.
Detailed record list
Occurred At
2020-05-08 10:53:00
Year
2020
Report Received Date
2020-06-05 00:00:00
Iyear
2020.0
Report Number
20200053.0
Supplemental Number
34121.0
Report Type
Supplemental Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2020-05-08 10:53:00
Location Street Address
8424 Santa Monica Blvd
Location City Name
West Hollywood
Location County Name
Los Angeles
Location State Abbreviation
CA
Location Postal Code
90069
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-05-08 22:03:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
24.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-05-08 10:53:00
On Site Datetime
2020-05-08 11:19:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
45.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1983.0
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Steel Seam Type Details
Seamless
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
0.3
Puncture Circum
0.3
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
3000.0
Est Cost Emergency
53900.0
Est Cost Other
0.0
Est Cost Unintentional Release
145.0
Prpty
57045.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
35.0
Normal Psig
35.0
Mop Psig
40.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
A201040862
One Call Center Name
Digalert
Locator Type
Utility Owner
Visible Marks
No
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
A** M****
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
A*****@s*******.com
Preparer Telephone
909-919-0463
Authorizer Name
A** M****
Authorizer Title
Pipeline Safety And Compliance Advisor
Authorizer Telephone
909-919-0463
Authorizer Email
A*****@s*******.com
Narrative
On may 8, 2020, a third-party contractor damaged a 6-inch steel gas main while boring to install conduit. Socalgas crews responded and controlled the gas with pressure control equipment. There were no injuries or further damage resulting from this incident. The 6-inch main was repaired by welding a wedding band. Investigation of the incident showed that there was a valid USA ticket, however, the 6-inch main was not marked out by the locator. Ticket had been left open in "project" status by the locator to return on a later date to complete. The locator did not address the ticket before the due date upon his return to work from his time off (7 days). This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.
Occurred At 2020-05-08 10:53:00
Year 2020
Report Received Date 2020-06-05 00:00:00
Iyear 2020.0
Report Number 20200053.0
Supplemental Number 34121.0
Report Type Supplemental Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2020-05-08 10:53:00
Location Street Address 8424 Santa Monica Blvd
Location City Name West Hollywood
Location County Name Los Angeles
Location State Abbreviation CA
Location Postal Code 90069
Location Latitude 34.090417 Google Maps OpenStreetMap
Location Longitude -118.374357 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-05-08 22:03:00
Nrc Rpt Num 1276942 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 24.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-05-08 10:53:00
On Site Datetime 2020-05-08 11:19:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 45.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1983.0
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Steel Seam Type Details Seamless
Wt Steel 0.188
Release Type Mechanical Puncture
Puncture Axial 0.3
Puncture Circum 0.3
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 3000.0
Est Cost Emergency 53900.0
Est Cost Other 0.0
Est Cost Unintentional Release 145.0
Prpty 57045.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 35.0
Normal Psig 35.0
Mop Psig 40.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num A201040862
One Call Center Name Digalert
Locator Type Utility Owner
Visible Marks No
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Locator Error
Preparer Name A** M****
Preparer Title Pipeline Safety And Compliance Advisor
Preparer Email A*****@s*******.com
Preparer Telephone 909-919-0463
Authorizer Name A** M****
Authorizer Title Pipeline Safety And Compliance Advisor
Authorizer Telephone 909-919-0463
Authorizer Email A*****@s*******.com
Narrative On may 8, 2020, a third-party contractor damaged a 6-inch steel gas main while boring to install conduit. Socalgas crews responded and controlled the gas with pressure control equipment. There were no injuries or further damage resulting from this incident. The 6-inch main was repaired by welding a wedding band. Investigation of the incident showed that there was a valid USA ticket, however, the 6-inch main was not marked out by the locator. Ticket had been left open in "project" status by the locator to return on a later date to complete. The locator did not address the ticket before the due date upon his return to work from his time off (7 days). This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. For any further questions, contact ali matin at (909) 919-0463.

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