GD incident on 2020-04-29 — PA

Operator
Peoples Natural Gas Company Llc
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-04-29 09:40
Report number
Location
PA, INDIANA
Narrative
During a routine annual inspection of district regulator station ls-260, peoples employees needed to isolate the regulator from the system in order to inspect it. In order to isolate that regulator, the station by-pass needs to be manually operated to maintain outlet pressure. The employees placed a gauge on the relief valve piping, which was upstream and now isolated from the outlet/downstream piping. While manually operating the station's by-pass they were unable to monitor the outlet pressure, resulting in an over pressurization of the downstream system in the town of robinson, pa. Supplemental question asked by nrc: were the employees involved with this incident re-qualified on the tasks that led to the over pressurization? On april 29, 2020, there were three employees on site performing the annual inspection of district regulator station ls-260, robinson, pa when the over pressurization occurred. All three individuals were re-qualified on june 23, 2020 on the tasks that led to that over pressurization. During the time period from 4/29/2020 until their re-qualification on 6/23/2020, none of these individuals were permitted to perform annual district regulator inspections independently, but were assigned to work with senior district regulator oq certified specialists.
Detailed record list
Occurred At
2020-04-29 09:40:00
Year
2020
Report Received Date
2020-05-29 00:00:00
Iyear
2020.0
Report Number
20200052.0
Supplemental Number
34663.0
Report Type
Supplemental Final
Operator Id
Name
Peoples Natural Gas Company Llc
Operator Street Address
375 North Shore Drive Suite 600
Operator City Name
Pittsburgh
Operator State Abbreviation
PA
Operator Postal Code
15212
Local Datetime
2020-04-29 09:40:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Street Address
111 Jefferson Street
Location City Name
Robinson
Location County Name
Indiana
Location State Abbreviation
PA
Location Postal Code
15949
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Nrc Rpt Datetime
2020-04-30 16:58:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
0.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-04-29 09:40:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2020-04-29 12:05:00
On Site Datetime
2020-04-29 09:40:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
District Regulator/metering Station
Installation Year
1981.0
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Other
Release Type Details
Over Pressurization. No Release Of Gas.
Class Location Type
Class 2 Location
Est Cost Oper Paid
47958.0
Est Cost Prop Damage
0.0
Est Cost Emergency
101840.0
Est Cost Other
0.0
Gas Cost In Mcf
7.7621
Est Cost Unintentional Release
0.0
Est Cost Intentional Release
0.0
Prpty
149798.0
Commercial Affected
2.0
Industrial Affected
0.0
Residences Affected
219.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
219.0
Num Business Building Affctd
2.0
Accident Psig
1.63
Normal Psig
0.5
Mop Psig
1.0
Mop Cfr Section
Maop Established Date
2015-11-23 00:00:00
Accident Pressure
Pressure Exceeded The Applicable Allowance In 192.201
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.7
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
Yes
Num Employees Tested
3
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D***** P* K****
Preparer Title
Manager Process Work Management
Preparer Email
D***********@p**********.com
Preparer Telephone
724-444-3251
Local Contact Name
D***** P* K****
Local Contact Email
D***********@p**********.com
Local Contact Telephone
724-444-3251
Authorizer Name
J***** A* G********
Authorizer Title
Sr. Vice President Rates - Regulatory Affairs
Authorizer Telephone
412-208-7905
Authorizer Email
J*****************@p**********.com
Narrative
During a routine annual inspection of district regulator station ls-260, peoples employees needed to isolate the regulator from the system in order to inspect it. In order to isolate that regulator, the station by-pass needs to be manually operated to maintain outlet pressure. The employees placed a gauge on the relief valve piping, which was upstream and now isolated from the outlet/downstream piping. While manually operating the station's by-pass they were unable to monitor the outlet pressure, resulting in an over pressurization of the downstream system in the town of robinson, pa. Supplemental question asked by nrc: were the employees involved with this incident re-qualified on the tasks that led to the over pressurization? On april 29, 2020, there were three employees on site performing the annual inspection of district regulator station ls-260, robinson, pa when the over pressurization occurred. All three individuals were re-qualified on june 23, 2020 on the tasks that led to that over pressurization. During the time period from 4/29/2020 until their re-qualification on 6/23/2020, none of these individuals were permitted to perform annual district regulator inspections independently, but were assigned to work with senior district regulator oq certified specialists.
Occurred At 2020-04-29 09:40:00
Year 2020
Report Received Date 2020-05-29 00:00:00
Iyear 2020.0
Report Number 20200052.0
Supplemental Number 34663.0
Report Type Supplemental Final
Operator Id 15350 PHMSA Enforcement
Name Peoples Natural Gas Company Llc
Operator Street Address 375 North Shore Drive Suite 600
Operator City Name Pittsburgh
Operator State Abbreviation PA
Operator Postal Code 15212
Local Datetime 2020-04-29 09:40:00
Time Zone Eastern
Daylight Savings Ind No
Location Street Address 111 Jefferson Street
Location City Name Robinson
Location County Name Indiana
Location State Abbreviation PA
Location Postal Code 15949
Location Latitude 40.399493 Google Maps OpenStreetMap
Location Longitude -79.145934 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Nrc Rpt Datetime 2020-04-30 16:58:00
Nrc Rpt Num 1276429 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 0.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-04-29 09:40:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2020-04-29 12:05:00
On Site Datetime 2020-04-29 09:40:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved District Regulator/metering Station
Installation Year 1981.0
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Other
Release Type Details Over Pressurization. No Release Of Gas.
Class Location Type Class 2 Location
Est Cost Oper Paid 47958.0
Est Cost Prop Damage 0.0
Est Cost Emergency 101840.0
Est Cost Other 0.0
Gas Cost In Mcf 7.7621
Est Cost Unintentional Release 0.0
Est Cost Intentional Release 0.0
Prpty 149798.0
Commercial Affected 2.0
Industrial Affected 0.0
Residences Affected 219.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 219.0
Num Business Building Affctd 2.0
Accident Psig 1.63
Normal Psig 0.5
Mop Psig 1.0
Mop Cfr Section 192.623 View CFR 49 §192
Maop Established Date 2015-11-23 00:00:00
Accident Pressure Pressure Exceeded The Applicable Allowance In 192.201
Gas Odorized System Type Injection Pump
Gas Odorized Level 0.7
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind Yes
Num Employees Tested 3
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D***** P* K****
Preparer Title Manager Process Work Management
Preparer Email D***********@p**********.com
Preparer Telephone 724-444-3251
Local Contact Name D***** P* K****
Local Contact Email D***********@p**********.com
Local Contact Telephone 724-444-3251
Authorizer Name J***** A* G********
Authorizer Title Sr. Vice President Rates - Regulatory Affairs
Authorizer Telephone 412-208-7905
Authorizer Email J*****************@p**********.com
Narrative During a routine annual inspection of district regulator station ls-260, peoples employees needed to isolate the regulator from the system in order to inspect it. In order to isolate that regulator, the station by-pass needs to be manually operated to maintain outlet pressure. The employees placed a gauge on the relief valve piping, which was upstream and now isolated from the outlet/downstream piping. While manually operating the station's by-pass they were unable to monitor the outlet pressure, resulting in an over pressurization of the downstream system in the town of robinson, pa. Supplemental question asked by nrc: were the employees involved with this incident re-qualified on the tasks that led to the over pressurization? On april 29, 2020, there were three employees on site performing the annual inspection of district regulator station ls-260, robinson, pa when the over pressurization occurred. All three individuals were re-qualified on june 23, 2020 on the tasks that led to that over pressurization. During the time period from 4/29/2020 until their re-qualification on 6/23/2020, none of these individuals were permitted to perform annual district regulator inspections independently, but were assigned to work with senior district regulator oq certified specialists.

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