GTG incident on 2020-04-14 — TX

Operator
Panhandle Eastern Pipeline Co
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-04-14 09:00
Report number
Location
TX
Narrative
While conducting an esd test the station vented 3.8 mmscf of natural gas. During a normal esd, it takes some time to blowdown the yard piping after activation of the system. When the blowdown valve continued to blow, operations personnel began to investigate and found the 300 suction side gate valve to still be open. The isolation valve under the blowdown valve was closed. Operations personnel isolated the suction side gate valve, then tested the valve and it operated as designed. Operations personnel tested the esd system and found there was an air leak on the esd tubing. The air leak was repaired and the system was tested.
Detailed record list
Report Received Date
2020-05-14 00:00:00
Iyear
2020
Report Number
20200051
Supplemental Number
33756
Report Type
Original Final
Operator Id
Name
Panhandle Eastern Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-04-14 09:20:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2020-04-14 09:38:00
Additional Nrc Report Numbers
1275497
Commodity Released Type
Natural Gas
Unintentional Release
3800
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Routine Test Was Being Conducted On Esd System.
Communication State Fed Ind
No
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2020-04-14 09:00:00
On Site Datetime
2020-04-14 08:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Il
Onshore Postal Code
62366
Onshore City Name
Pleasant Hill
Onshore County Name
Pike
Designated Location
Not Applicable
Pipe Fac Name
Pleasant Hill Compressor Station
Segment Name
300 Discharge Relief
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Esd System, But Excluding Product Drain Lines And Tubing
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Air Leak On Esd Tubing Prevented Esd Signal Pressure From Reaching The Trip Point Of The Valve. The Valve Didn't Close To Isolate The Gas Flow To The Relief Valve.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
179
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
8664
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
2.28
Prpty
8664
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
500
Gas Flow In Pipe In Mcf
350
Mop Psig
900
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1954-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operations personnel were conducting an esd test and had notified the control room prior to testing.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Eq Failure Details
An Air Leak On The Esd Signal Tubing Prevented The Pressure From Building Up High Enough To Trip The 300 Suction Side Gate Valve.
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring And Poppets Prematurely Reached End Of Life.
Preparer Name
K***** H*******
Preparer Title
Senior Specialist Regulatory Compliance
Preparer Email
K***************@e*************.com
Preparer Telephone
713-989-7085
Authorizer Name
D**** N******
Authorizer Title
Senior Director Regulatory Compliance
Authorizer Telephone
713-989-7232
Authorizer Email
D************@e*************.com
Narrative
While conducting an esd test the station vented 3.8 mmscf of natural gas. During a normal esd, it takes some time to blowdown the yard piping after activation of the system. When the blowdown valve continued to blow, operations personnel began to investigate and found the 300 suction side gate valve to still be open. The isolation valve under the blowdown valve was closed. Operations personnel isolated the suction side gate valve, then tested the valve and it operated as designed. Operations personnel tested the esd system and found there was an air leak on the esd tubing. The air leak was repaired and the system was tested.
Report Received Date 2020-05-14 00:00:00
Iyear 2020
Report Number 20200051
Supplemental Number 33756
Report Type Original Final
Operator Id 15105 PHMSA Enforcement
Name Panhandle Eastern Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-04-14 09:20:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 39.47196 Google Maps OpenStreetMap
Location Longitude -90.9141 Google Maps OpenStreetMap
Nrc Rpt Num 1275372 NRC Report How to search
Nrc Rpt Datetime 2020-04-14 09:38:00
Additional Nrc Report Numbers 1275497
Commodity Released Type Natural Gas
Unintentional Release 3800
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Routine Test Was Being Conducted On Esd System.
Communication State Fed Ind No
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2020-04-14 09:00:00
On Site Datetime 2020-04-14 08:00:00
On Off Shore Onshore
Onshore State Abbreviation Il
Onshore Postal Code 62366
Onshore City Name Pleasant Hill
Onshore County Name Pike
Designated Location Not Applicable
Pipe Fac Name Pleasant Hill Compressor Station
Segment Name 300 Discharge Relief
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Esd System, But Excluding Product Drain Lines And Tubing
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Air Leak On Esd Tubing Prevented Esd Signal Pressure From Reaching The Trip Point Of The Valve. The Valve Didn't Close To Isolate The Gas Flow To The Relief Valve.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 179
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 8664
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 2.28
Prpty 8664
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 500
Gas Flow In Pipe In Mcf 350
Mop Psig 900
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1954-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operations personnel were conducting an esd test and had notified the control room prior to testing.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Eq Failure Details An Air Leak On The Esd Signal Tubing Prevented The Pressure From Building Up High Enough To Trip The 300 Suction Side Gate Valve.
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring And Poppets Prematurely Reached End Of Life.
Preparer Name K***** H*******
Preparer Title Senior Specialist Regulatory Compliance
Preparer Email K***************@e*************.com
Preparer Telephone 713-989-7085
Authorizer Name D**** N******
Authorizer Title Senior Director Regulatory Compliance
Authorizer Telephone 713-989-7232
Authorizer Email D************@e*************.com
Narrative While conducting an esd test the station vented 3.8 mmscf of natural gas. During a normal esd, it takes some time to blowdown the yard piping after activation of the system. When the blowdown valve continued to blow, operations personnel began to investigate and found the 300 suction side gate valve to still be open. The isolation valve under the blowdown valve was closed. Operations personnel isolated the suction side gate valve, then tested the valve and it operated as designed. Operations personnel tested the esd system and found there was an air leak on the esd tubing. The air leak was repaired and the system was tested.

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