GD incident on 2020-04-18 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$38,000
Incident datetime
2020-04-18 10:53
Report number
Location
TX, TARRANT
Narrative
On april 18, 2020, the grand prairie fire department notified atmos energy of a natural gas leak in front of 3051 e. Mayfield in grand prairie, texas. The fire department secured the scene and closed off traffic near the leak. While atmos crews were en route, a vehicle entered the secured area and parked over the leak resulting in an ignition of the gas. The grand prairie police department moved the vehicle away from the leak. The city of grand prairie emergency management conducted evacuations via text and email and therefore is unable to provide an estimate of the number of general public evacuated. A current estimate of third party property damage and operator costs has been included in part d. However, all costs associated with this incident are still in the process of being compiled. Atmos energy crews began work to isolate and repair the leak. The leak was secured at 6:30 pm and the pipeline was placed back in service at 4:00 pm on monday, april 20, 2020. 48-hour update nrc# 1275699.
Detailed record list
Occurred At
2020-04-18 10:53:00
Year
2020
Report Received Date
2020-05-18 00:00:00
Iyear
2020.0
Report Number
20200050.0
Supplemental Number
34820.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2020-04-18 12:30:00
Time Zone
Central
Daylight Savings Ind
No
Location Street Address
3051 E. Mayfield & Watson Rd (Hwy 360)
Location City Name
Grand Prairie
Location County Name
Tarrant
Location State Abbreviation
TX
Location Postal Code
75052-7330
Location Latitude
Location Longitude
-97.06108939
Flow Cont Key Crit Ind
Yes
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2020-04-18 13:02:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
3140.5
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Ignite Datetime
2020-04-18 10:53:00
How Extinguished
Allowed To Burn Out
Gas Consumed By Fire In Mcf
2643.1
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-04-18 10:53:00
On Site Datetime
2020-04-18 12:30:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
45.0
Other Underground Facilities
No
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1977.0
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic Unknown Ind
Unknown
Material Pe Pipe Code
Unknown
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
18.8
Rupture Width
2
Class Location Type
Class 3 Location
Est Cost Oper Paid
175867.0
Est Cost Prop Damage
38000.0
Est Cost Emergency
14133.0
Est Cost Other
32336.0
Est Cost Other Details
Fire Department Hazmat Response.
Gas Cost In Mcf
3.85
Est Cost Unintentional Release
12091.0
Est Cost Intentional Release
0.0
Prpty
272427.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
15.0
Num Business Building Affctd
6.0
Accident Psig
31.0
Normal Psig
35.0
Mop Psig
50.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1977-09-22 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Fusion Joint
Pwjf Failure Type
Fusion Joint
Plastic Joint Subtype
Butt, Heat Fusion
Fpw Installed Year
1977
Fpw First Plastic Type
Polyethylene (Pe)
Fpw Second Plastic Type
Polyethylene (Pe)
Additional Lack Fusion Ind
Yes
Result Construction Ind
Yes
Result Construction Subtype
Poor Workmanship
Hydrotest Conducted Ind
No
Preparer Name
B**** M**********
Preparer Title
Operations Supervisor
Preparer Email
B****************@a**********.com
Preparer Telephone
214-206-2387
Local Contact Name
B**** M**********
Local Contact Email
B****************@a**********.com
Local Contact Telephone
214-206-2387
Authorizer Name
M**** S*****
Authorizer Title
V.p. Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
On april 18, 2020, the grand prairie fire department notified atmos energy of a natural gas leak in front of 3051 e. Mayfield in grand prairie, texas. The fire department secured the scene and closed off traffic near the leak. While atmos crews were en route, a vehicle entered the secured area and parked over the leak resulting in an ignition of the gas. The grand prairie police department moved the vehicle away from the leak. The city of grand prairie emergency management conducted evacuations via text and email and therefore is unable to provide an estimate of the number of general public evacuated. A current estimate of third party property damage and operator costs has been included in part d. However, all costs associated with this incident are still in the process of being compiled. Atmos energy crews began work to isolate and repair the leak. The leak was secured at 6:30 pm and the pipeline was placed back in service at 4:00 pm on monday, april 20, 2020. 48-hour update nrc# 1275699.
Occurred At 2020-04-18 10:53:00
Year 2020
Report Received Date 2020-05-18 00:00:00
Iyear 2020.0
Report Number 20200050.0
Supplemental Number 34820.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2020-04-18 12:30:00
Time Zone Central
Daylight Savings Ind No
Location Street Address 3051 E. Mayfield & Watson Rd (Hwy 360)
Location City Name Grand Prairie
Location County Name Tarrant
Location State Abbreviation TX
Location Postal Code 75052-7330
Location Latitude 32.69147696 Google Maps OpenStreetMap
Location Longitude -97.06108939 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Datetime 2020-04-18 13:02:00
Nrc Rpt Num 1275628 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 3140.5
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Ignite Datetime 2020-04-18 10:53:00
How Extinguished Allowed To Burn Out
Gas Consumed By Fire In Mcf 2643.1
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-04-18 10:53:00
On Site Datetime 2020-04-18 12:30:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 45.0
Other Underground Facilities No
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1977.0
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic Unknown Ind Unknown
Material Pe Pipe Code Unknown
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 18.8
Rupture Width 2
Class Location Type Class 3 Location
Est Cost Oper Paid 175867.0
Est Cost Prop Damage 38000.0
Est Cost Emergency 14133.0
Est Cost Other 32336.0
Est Cost Other Details Fire Department Hazmat Response.
Gas Cost In Mcf 3.85
Est Cost Unintentional Release 12091.0
Est Cost Intentional Release 0.0
Prpty 272427.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 15.0
Num Business Building Affctd 6.0
Accident Psig 31.0
Normal Psig 35.0
Mop Psig 50.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1977-09-22 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Fusion Joint
Pwjf Failure Type Fusion Joint
Plastic Joint Subtype Butt, Heat Fusion
Fpw Installed Year 1977
Fpw First Plastic Type Polyethylene (Pe)
Fpw Second Plastic Type Polyethylene (Pe)
Additional Lack Fusion Ind Yes
Result Construction Ind Yes
Result Construction Subtype Poor Workmanship
Hydrotest Conducted Ind No
Preparer Name B**** M**********
Preparer Title Operations Supervisor
Preparer Email B****************@a**********.com
Preparer Telephone 214-206-2387
Local Contact Name B**** M**********
Local Contact Email B****************@a**********.com
Local Contact Telephone 214-206-2387
Authorizer Name M**** S*****
Authorizer Title V.p. Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative On april 18, 2020, the grand prairie fire department notified atmos energy of a natural gas leak in front of 3051 e. Mayfield in grand prairie, texas. The fire department secured the scene and closed off traffic near the leak. While atmos crews were en route, a vehicle entered the secured area and parked over the leak resulting in an ignition of the gas. The grand prairie police department moved the vehicle away from the leak. The city of grand prairie emergency management conducted evacuations via text and email and therefore is unable to provide an estimate of the number of general public evacuated. A current estimate of third party property damage and operator costs has been included in part d. However, all costs associated with this incident are still in the process of being compiled. Atmos energy crews began work to isolate and repair the leak. The leak was secured at 6:30 pm and the pipeline was placed back in service at 4:00 pm on monday, april 20, 2020. 48-hour update nrc# 1275699.

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