GD incident on 2020-03-05 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Equipment Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-03-05 09:30
Report number
Location
TX, CORYELL
Narrative
At 9:30 am on march 5, 2020, a threaded fitting failed at a connection point with a 2" brass ball valve at ground level on a recently installed temporary bypass at the copperas cove city gate station, causing an interruption in service. The failure of the threaded connection on the temporary bypass valve occurred during support cribbing adjustment. Atmos energy identified additional potential contributing factors as the valve material and possible under-torqueing of the threaded connection. An initial estimate of the copperas cove system based on the facts available at that time resulted in an underestimation of the total number of customers and the cost of relights. However, a subsequent review of outage reports when refining that estimate indicated that the customer outage was more extensive than originally anticipated. At 12:30 pm, the relight costs were estimated to be greater than $50,000, and a telephonic report was made to the national response center at 12:51 pm. Gas service was interrupted to 270 commercial and 4067 residential customers. The appropriate repairs were made and the facility was restarted at 12:12 am on march 6, 2020. Service has been restored to all affected customers. 48 hr. Nrc # 1272905
Detailed record list
Occurred At
2020-03-05 09:30:00
Year
2020
Report Received Date
2020-04-03 00:00:00
Iyear
2020.0
Report Number
20200041.0
Supplemental Number
34100.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2020-03-05 09:30:00
Location Street Address
2707 Us Hwy 190
Location City Name
Copperas Cove
Location County Name
Coryell
Location State Abbreviation
TX
Location Postal Code
76522
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-03-05 11:51:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
51.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-03-05 09:30:00
On Site Datetime
2020-03-05 10:00:00
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
District Regulator/metering Station
Installation Year
2020.0
Material Involved
Other
Material Details
Brass Ball Valve To Steel Pipe Nipple
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
0.0
Est Cost Emergency
412485.0
Est Cost Other
0.0
Est Cost Unintentional Release
187.0
Prpty
412672.0
Commercial Affected
270.0
Industrial Affected
0.0
Residences Affected
4067.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
40.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident not related to control room operation
Employee Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
8
Num Contractors Failed
0
Cause
Equipment Failure
Cause Details
Threaded Connection Failure
Eq Failure Type
Threaded Connection Failure
Other Stripped Ind
Threaded Fitting
Preparer Name
D*** G*******
Preparer Title
Compliance Supervisor
Preparer Email
D************@a**********.com
Preparer Telephone
512-844-8270
Preparer Fax
512-310-3880
Authorizer Name
M**** S*****
Authorizer Title
Vice President Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
At 9:30 am on march 5, 2020, a threaded fitting failed at a connection point with a 2" brass ball valve at ground level on a recently installed temporary bypass at the copperas cove city gate station, causing an interruption in service. The failure of the threaded connection on the temporary bypass valve occurred during support cribbing adjustment. Atmos energy identified additional potential contributing factors as the valve material and possible under-torqueing of the threaded connection. An initial estimate of the copperas cove system based on the facts available at that time resulted in an underestimation of the total number of customers and the cost of relights. However, a subsequent review of outage reports when refining that estimate indicated that the customer outage was more extensive than originally anticipated. At 12:30 pm, the relight costs were estimated to be greater than $50,000, and a telephonic report was made to the national response center at 12:51 pm. Gas service was interrupted to 270 commercial and 4067 residential customers. The appropriate repairs were made and the facility was restarted at 12:12 am on march 6, 2020. Service has been restored to all affected customers. 48 hr. Nrc # 1272905
Occurred At 2020-03-05 09:30:00
Year 2020
Report Received Date 2020-04-03 00:00:00
Iyear 2020.0
Report Number 20200041.0
Supplemental Number 34100.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2020-03-05 09:30:00
Location Street Address 2707 Us Hwy 190
Location City Name Copperas Cove
Location County Name Coryell
Location State Abbreviation TX
Location Postal Code 76522
Location Latitude 31.12097 Google Maps OpenStreetMap
Location Longitude -97.8713 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-03-05 11:51:00
Nrc Rpt Num 1272777 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 51.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-03-05 09:30:00
On Site Datetime 2020-03-05 10:00:00
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved District Regulator/metering Station
Installation Year 2020.0
Material Involved Other
Material Details Brass Ball Valve To Steel Pipe Nipple
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 0.0
Est Cost Emergency 412485.0
Est Cost Other 0.0
Est Cost Unintentional Release 187.0
Prpty 412672.0
Commercial Affected 270.0
Industrial Affected 0.0
Residences Affected 4067.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 40.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident not related to control room operation
Employee Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 8
Num Contractors Failed 0
Cause Equipment Failure
Cause Details Threaded Connection Failure
Eq Failure Type Threaded Connection Failure
Other Stripped Ind Threaded Fitting
Preparer Name D*** G*******
Preparer Title Compliance Supervisor
Preparer Email D************@a**********.com
Preparer Telephone 512-844-8270
Preparer Fax 512-310-3880
Authorizer Name M**** S*****
Authorizer Title Vice President Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative At 9:30 am on march 5, 2020, a threaded fitting failed at a connection point with a 2" brass ball valve at ground level on a recently installed temporary bypass at the copperas cove city gate station, causing an interruption in service. The failure of the threaded connection on the temporary bypass valve occurred during support cribbing adjustment. Atmos energy identified additional potential contributing factors as the valve material and possible under-torqueing of the threaded connection. An initial estimate of the copperas cove system based on the facts available at that time resulted in an underestimation of the total number of customers and the cost of relights. However, a subsequent review of outage reports when refining that estimate indicated that the customer outage was more extensive than originally anticipated. At 12:30 pm, the relight costs were estimated to be greater than $50,000, and a telephonic report was made to the national response center at 12:51 pm. Gas service was interrupted to 270 commercial and 4067 residential customers. The appropriate repairs were made and the facility was restarted at 12:12 am on march 6, 2020. Service has been restored to all affected customers. 48 hr. Nrc # 1272905

All rights reserved. Copyright © by ClearPHMSA