HL incident on 2020-01-14 — KS

Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2020-01-14 23:21
Report number
Location
KS
Narrative
At 10:20 pm cst, the controller noticed that the meade booster pump bp-3201 did not appear to be putting up enough pressure and flow to be functioning properly. The controller shut down the pump, attempted one restart, per jayhawk pipeline procedures, and immediately shut the pump back down/isolated it from the system. The controller notified appropriate personnel and mobilized field staff to the pump station to investigate. Upon arrival at the pump station, field staff confirmed that the pump seal failed and had released approximately 4.6 barrels of product to the tank dike. 100% of the product was contained on the operator controlled property. The pump was replaced and the system returned to service the following day. Kdhe was notified of the incident. The nrc reporting thresholds were not met as a result of this incident.
Detailed record list
Report Received Date
2020-02-04 00:00:00
Iyear
2020
Report Number
20200033
Supplemental Number
34780
Report Type
Supplemental Final
Operator Id
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 S. Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2020-01-14 23:17:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4.6
Recovered Bbls
4.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2020-01-14 23:21:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-01-14 22:23:00
Restart Datetime
2020-01-15 14:58:00
On Site Datetime
2020-01-14 23:21:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Meade Station
Segment Name
Meade To Harper
Onshore State Abbreviation
Ks
Onshore Postal Code
67869
Onshore City Name
Not Within A Municipality
Onshore County Name
Meade
Designated Location
Milepost/valve Station
Designated Name
Meade Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
250
Est Cost Prop Damage
10000
Est Cost Emergency
10000
Est Cost Environmental
9000
Est Cost Other
500
Est Cost Other Details
Costs To Compile Phsma Report.
Prpty
29750
Accident Psig
3
Mop Psig
403
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
No Additional Factors Were Found To Have Contributed To This Incident
Preparer Name
M******* S*****
Preparer Title
Manager Dot Compliance
Preparer Email
M**************@c*****.com
Preparer Telephone
4066285200
Prepared Date
2021-01-28 00:00:00
Authorizer Name
G****** B****
Authorizer Telephone
4066285200
Authorizer Title
Vp Pipelines And Terminals
Authorizer Email
G*********@c*****.com
Narrative
At 10:20 pm cst, the controller noticed that the meade booster pump bp-3201 did not appear to be putting up enough pressure and flow to be functioning properly. The controller shut down the pump, attempted one restart, per jayhawk pipeline procedures, and immediately shut the pump back down/isolated it from the system. The controller notified appropriate personnel and mobilized field staff to the pump station to investigate. Upon arrival at the pump station, field staff confirmed that the pump seal failed and had released approximately 4.6 barrels of product to the tank dike. 100% of the product was contained on the operator controlled property. The pump was replaced and the system returned to service the following day. Kdhe was notified of the incident. The nrc reporting thresholds were not met as a result of this incident.
Report Received Date 2020-02-04 00:00:00
Iyear 2020
Report Number 20200033
Supplemental Number 34780
Report Type Supplemental Final
Operator Id 9175 PHMSA Enforcement
Name Jayhawk Pipeline Llc
Operator Street Address 2000 S. Main
Operator City Name Mcpherson
Operator State Abbreviation KS
Operator Postal Code 67460
Local Datetime 2020-01-14 23:17:00
Location Latitude 37.139861 Google Maps OpenStreetMap
Location Longitude -100.569356 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4.6
Recovered Bbls 4.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2020-01-14 23:21:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-01-14 22:23:00
Restart Datetime 2020-01-15 14:58:00
On Site Datetime 2020-01-14 23:21:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Meade Station
Segment Name Meade To Harper
Onshore State Abbreviation Ks
Onshore Postal Code 67869
Onshore City Name Not Within A Municipality
Onshore County Name Meade
Designated Location Milepost/valve Station
Designated Name Meade Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 250
Est Cost Prop Damage 10000
Est Cost Emergency 10000
Est Cost Environmental 9000
Est Cost Other 500
Est Cost Other Details Costs To Compile Phsma Report.
Prpty 29750
Accident Psig 3
Mop Psig 403
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details No Additional Factors Were Found To Have Contributed To This Incident
Preparer Name M******* S*****
Preparer Title Manager Dot Compliance
Preparer Email M**************@c*****.com
Preparer Telephone 4066285200
Prepared Date 2021-01-28 00:00:00
Authorizer Name G****** B****
Authorizer Telephone 4066285200
Authorizer Title Vp Pipelines And Terminals
Authorizer Email G*********@c*****.com
Narrative At 10:20 pm cst, the controller noticed that the meade booster pump bp-3201 did not appear to be putting up enough pressure and flow to be functioning properly. The controller shut down the pump, attempted one restart, per jayhawk pipeline procedures, and immediately shut the pump back down/isolated it from the system. The controller notified appropriate personnel and mobilized field staff to the pump station to investigate. Upon arrival at the pump station, field staff confirmed that the pump seal failed and had released approximately 4.6 barrels of product to the tank dike. 100% of the product was contained on the operator controlled property. The pump was replaced and the system returned to service the following day. Kdhe was notified of the incident. The nrc reporting thresholds were not met as a result of this incident.

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