GD incident on 2020-01-28 — GA

Operator
Atlanta Gas Light Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2020-01-28 11:08
Report number
Location
GA, FULTON
Narrative
A 4-inch plastic natural gas main was ruptured by a contract crew while installing telecommunications conduit by directional drilling. Once the incident was made safe it was identified that the fire department had stopped the railroad for more than the 20-minute threshold the company has in its operations procedure manual (opm) for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made, however, it appears the locate ticket had expired and the marks at the job site were faded. In addition, the faded marks appeared to be mis-located by approximately 6-inches where the excavator had failed to pothole to determine the proximity of the pipeline. Additional nrc report number 1269835 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Detailed record list
Occurred At
2020-01-28 11:08:00
Year
2020
Report Received Date
2020-02-25 00:00:00
Iyear
2020.0
Report Number
20200028.0
Supplemental Number
33370.0
Report Type
Original Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309
Local Datetime
2020-01-28 11:08:00
Location Street Address
Linkwood Rd At Martin Luther King Jr Rd
Location City Name
Atlanta
Location County Name
Fulton
Location State Abbreviation
GA
Location Postal Code
30311
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-01-28 14:16:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
162.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2020-01-28 11:08:00
On Site Datetime
2020-01-28 11:22:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2011.0
Pipe Diameter
4.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
2500.0
Est Cost Emergency
1500.0
Est Cost Other
0.0
Est Cost Unintentional Release
340.0
Prpty
4340.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
45.0
Normal Psig
45.0
Mop Psig
45.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
10309400026
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
6.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
R**** M*******
Preparer Title
Lead Compliance Engineer
Preparer Email
R*******@s*********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4710
Authorizer Name
R*** S*****
Authorizer Title
Director Compliance And Qa
Authorizer Telephone
(404) 584-4910
Authorizer Email
R******@s*********.com
Narrative
A 4-inch plastic natural gas main was ruptured by a contract crew while installing telecommunications conduit by directional drilling. Once the incident was made safe it was identified that the fire department had stopped the railroad for more than the 20-minute threshold the company has in its operations procedure manual (opm) for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made, however, it appears the locate ticket had expired and the marks at the job site were faded. In addition, the faded marks appeared to be mis-located by approximately 6-inches where the excavator had failed to pothole to determine the proximity of the pipeline. Additional nrc report number 1269835 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Occurred At 2020-01-28 11:08:00
Year 2020
Report Received Date 2020-02-25 00:00:00
Iyear 2020.0
Report Number 20200028.0
Supplemental Number 33370.0
Report Type Original Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309
Local Datetime 2020-01-28 11:08:00
Location Street Address Linkwood Rd At Martin Luther King Jr Rd
Location City Name Atlanta
Location County Name Fulton
Location State Abbreviation GA
Location Postal Code 30311
Location Latitude 33.754582 Google Maps OpenStreetMap
Location Longitude -84.481799 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-01-28 14:16:00
Nrc Rpt Num 1269775 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 162.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2020-01-28 11:08:00
On Site Datetime 2020-01-28 11:22:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2011.0
Pipe Diameter 4.0
Pipe Specification Astm D2513
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 2500.0
Est Cost Emergency 1500.0
Est Cost Other 0.0
Est Cost Unintentional Release 340.0
Prpty 4340.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 45.0
Normal Psig 45.0
Mop Psig 45.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num 10309400026
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 6.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name R**** M*******
Preparer Title Lead Compliance Engineer
Preparer Email R*******@s*********.com
Preparer Telephone (404) 584-3733
Preparer Fax (404) 584-4710
Authorizer Name R*** S*****
Authorizer Title Director Compliance And Qa
Authorizer Telephone (404) 584-4910
Authorizer Email R******@s*********.com
Narrative A 4-inch plastic natural gas main was ruptured by a contract crew while installing telecommunications conduit by directional drilling. Once the incident was made safe it was identified that the fire department had stopped the railroad for more than the 20-minute threshold the company has in its operations procedure manual (opm) for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made, however, it appears the locate ticket had expired and the marks at the job site were faded. In addition, the faded marks appeared to be mis-located by approximately 6-inches where the excavator had failed to pothole to determine the proximity of the pipeline. Additional nrc report number 1269835 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.

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