GD incident on 2020-01-22 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$80,883
Incident datetime
2020-01-22 12:00
Report number
Location
TX, DALLAS
Narrative
On the morning of january 22, 2020, pro bore construction was directional boring for telecommunications and hit a 12-inch poly main. The excavator had a valid locate ticket, 2050941166 and although the damage occurred in the scope of the locate ticket, the gas lines in the intersection were not marked. Atmos energy was notified of the damage by the fire department at 10:55 am. Tech arrived onsite around 11:44 am. Assistance arrived at 1:30 pm. The valve on the 12-inch line in the sw corner of the intersection was turned to the off position around 1:50 pm. The 4-inch poly line north of the intersection was squeezed off around 3:45 pm. Around 6:00 pm, the contractor arrived onsite to begin process of applying short stop to the 12-inch steel line east of the intersection. On january 23, 2020, the condition was eliminated around 7:11 am. Gas service was restored to the system after repairs around 12:00 pm on january 24, 2020. *48-hour update: nrc # 1269535.
Detailed record list
Occurred At
2020-01-22 12:00:00
Year
2020
Report Received Date
2020-02-17 00:00:00
Iyear
2020.0
Report Number
20200024.0
Supplemental Number
33869.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2020-01-22 12:00:00
Location Street Address
100 E Clarendon Dr
Location City Name
Dallas
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75203
Location Latitude
Location Longitude
-96.82257394
Nrc Rpt Datetime
2020-01-23 07:58:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
2163.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
33.0
Incident Identified Datetime
2020-01-22 12:00:00
On Site Datetime
2020-01-22 11:44:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
36.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2019.0
Pipe Diameter
12.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Performance Pipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic
1.159
Material Pe Pipe Code
4710
Release Type
Mechanical Puncture
Puncture Axial
2.5
Puncture Circum
2.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
80883.0
Est Cost Emergency
43408.0
Est Cost Other
0.0
Est Cost Unintentional Release
9731.0
Prpty
134022.0
Commercial Affected
4.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
24.0
Normal Psig
24.0
Mop Psig
55.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Public Util Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
2050939705
One Call Center Name
Texas811
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
19.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
P****** M******
Preparer Title
Manager Of Operations
Preparer Email
P***************@a**********.com
Preparer Telephone
2144267082
Authorizer Name
M**** S*****
Authorizer Title
Vice President Technical Services
Authorizer Telephone
2142062033
Authorizer Email
M***********@a**********.com
Narrative
On the morning of january 22, 2020, pro bore construction was directional boring for telecommunications and hit a 12-inch poly main. The excavator had a valid locate ticket, 2050941166 and although the damage occurred in the scope of the locate ticket, the gas lines in the intersection were not marked. Atmos energy was notified of the damage by the fire department at 10:55 am. Tech arrived onsite around 11:44 am. Assistance arrived at 1:30 pm. The valve on the 12-inch line in the sw corner of the intersection was turned to the off position around 1:50 pm. The 4-inch poly line north of the intersection was squeezed off around 3:45 pm. Around 6:00 pm, the contractor arrived onsite to begin process of applying short stop to the 12-inch steel line east of the intersection. On january 23, 2020, the condition was eliminated around 7:11 am. Gas service was restored to the system after repairs around 12:00 pm on january 24, 2020. *48-hour update: nrc # 1269535.
Occurred At 2020-01-22 12:00:00
Year 2020
Report Received Date 2020-02-17 00:00:00
Iyear 2020.0
Report Number 20200024.0
Supplemental Number 33869.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2020-01-22 12:00:00
Location Street Address 100 E Clarendon Dr
Location City Name Dallas
Location County Name Dallas
Location State Abbreviation TX
Location Postal Code 75203
Location Latitude 32.73449576 Google Maps OpenStreetMap
Location Longitude -96.82257394 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-01-23 07:58:00
Nrc Rpt Num 1269346 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 2163.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 33.0
Incident Identified Datetime 2020-01-22 12:00:00
On Site Datetime 2020-01-22 11:44:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 36.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2019.0
Pipe Diameter 12.0
Pipe Specification Astm D2513
Pipe Manufacturer Performance Pipe
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic 1.159
Material Pe Pipe Code 4710
Release Type Mechanical Puncture
Puncture Axial 2.5
Puncture Circum 2.5
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 80883.0
Est Cost Emergency 43408.0
Est Cost Other 0.0
Est Cost Unintentional Release 9731.0
Prpty 134022.0
Commercial Affected 4.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 24.0
Normal Psig 24.0
Mop Psig 55.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Public Util Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num 2050939705
One Call Center Name Texas811
Locator Type Contract Locator
Visible Marks No
Service Interruption Yes
Service Interruption Hours 19.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Locator Error
Preparer Name P****** M******
Preparer Title Manager Of Operations
Preparer Email P***************@a**********.com
Preparer Telephone 2144267082
Authorizer Name M**** S*****
Authorizer Title Vice President Technical Services
Authorizer Telephone 2142062033
Authorizer Email M***********@a**********.com
Narrative On the morning of january 22, 2020, pro bore construction was directional boring for telecommunications and hit a 12-inch poly main. The excavator had a valid locate ticket, 2050941166 and although the damage occurred in the scope of the locate ticket, the gas lines in the intersection were not marked. Atmos energy was notified of the damage by the fire department at 10:55 am. Tech arrived onsite around 11:44 am. Assistance arrived at 1:30 pm. The valve on the 12-inch line in the sw corner of the intersection was turned to the off position around 1:50 pm. The 4-inch poly line north of the intersection was squeezed off around 3:45 pm. Around 6:00 pm, the contractor arrived onsite to begin process of applying short stop to the 12-inch steel line east of the intersection. On january 23, 2020, the condition was eliminated around 7:11 am. Gas service was restored to the system after repairs around 12:00 pm on january 24, 2020. *48-hour update: nrc # 1269535.

All rights reserved. Copyright © by ClearPHMSA