GD incident on 2020-01-13 — CA

Operator
Southern California Gas Co
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,000
Incident datetime
2020-01-13 09:43
Report number
Location
CA, LOS ANGELES
Narrative
On 01/13/2020, socalgas was notified of a gas leak at 642 s alvarado street, los angeles. Socalgas crews were sent to the scene to perform leak investigation and centered leak over an 8-inch steel main. The leak was isolated by operating two mainline valves and gas was controlled at 05:25 on 01/14/2020. The leak was permanently repaired on 01/14/2020 by welding on a weld patch. All customer restores were completed on 01/15/2020. There were no injuries or further damages resulting from the release of gas. Further investigation shows the cause of leak was corrosion on bottom of main. A cathodic protection mitigation plan was developed to monitor the bell hole location until further remediation is determined. This incident was reported to DOT and cpuc due to gas release and damages exceeding $50,000. For any further questions, please contact ali matin at (909) 919-0463.
Detailed record list
Occurred At
2020-01-13 09:43:00
Year
2020
Report Received Date
2020-02-12 00:00:00
Iyear
2020.0
Report Number
20200021.0
Supplemental Number
33327.0
Report Type
Original Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2020-01-13 09:43:00
Location Street Address
642 S Alvarado Street
Location City Name
Los Angeles
Location County Name
Los Angeles
Location State Abbreviation
CA
Location Postal Code
90057
Location Latitude
Location Longitude
Nrc Rpt Datetime
2020-01-14 09:04:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
561.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
120.0
Incident Identified Datetime
2020-01-13 09:43:00
On Site Datetime
2020-01-13 09:43:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
57.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1933.0
Pipe Diameter
8.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Other
Leak Type Other
Corrosion On Band.
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
26000.0
Est Cost Emergency
14000.0
Est Cost Other
15000.0
Est Cost Other Details
Paving Costs.
Est Cost Unintentional Release
3366.0
Prpty
58366.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
35.0
Accident Psig
35.0
Normal Psig
35.0
Mop Psig
40.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Preliminary Indication Is Stray Current.
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
No
Shielding Evident
No
Cathodic Survey Type
No
Prior Damage
No
Coating Type
Coal Tar
Cor Hydrotest Leak Survey Date
2019-09-16 00:00:00
Cor Hydrotest Conducted Ind
No
Preparer Name
A** M****
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
A*****@s*******.com
Preparer Telephone
909-919-0463
Authorizer Name
A** M****
Authorizer Title
Pipeline Safety And Compliance Advisor
Authorizer Telephone
909-919-0463
Authorizer Email
A*****@s*******.com
Narrative
On 01/13/2020, socalgas was notified of a gas leak at 642 s alvarado street, los angeles. Socalgas crews were sent to the scene to perform leak investigation and centered leak over an 8-inch steel main. The leak was isolated by operating two mainline valves and gas was controlled at 05:25 on 01/14/2020. The leak was permanently repaired on 01/14/2020 by welding on a weld patch. All customer restores were completed on 01/15/2020. There were no injuries or further damages resulting from the release of gas. Further investigation shows the cause of leak was corrosion on bottom of main. A cathodic protection mitigation plan was developed to monitor the bell hole location until further remediation is determined. This incident was reported to DOT and cpuc due to gas release and damages exceeding $50,000. For any further questions, please contact ali matin at (909) 919-0463.
Occurred At 2020-01-13 09:43:00
Year 2020
Report Received Date 2020-02-12 00:00:00
Iyear 2020.0
Report Number 20200021.0
Supplemental Number 33327.0
Report Type Original Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2020-01-13 09:43:00
Location Street Address 642 S Alvarado Street
Location City Name Los Angeles
Location County Name Los Angeles
Location State Abbreviation CA
Location Postal Code 90057
Location Latitude 34.057975 Google Maps OpenStreetMap
Location Longitude -118.275783 Google Maps OpenStreetMap
Nrc Rpt Datetime 2020-01-14 09:04:00
Nrc Rpt Num 1268662 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 561.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 120.0
Incident Identified Datetime 2020-01-13 09:43:00
On Site Datetime 2020-01-13 09:43:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 57.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1933.0
Pipe Diameter 8.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Leak
Leak Type Other
Leak Type Other Corrosion On Band.
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 26000.0
Est Cost Emergency 14000.0
Est Cost Other 15000.0
Est Cost Other Details Paving Costs.
Est Cost Unintentional Release 3366.0
Prpty 58366.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 35.0
Accident Psig 35.0
Normal Psig 35.0
Mop Psig 40.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Preliminary Indication Is Stray Current.
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind No
Shielding Evident No
Cathodic Survey Type No
Prior Damage No
Coating Type Coal Tar
Cor Hydrotest Leak Survey Date 2019-09-16 00:00:00
Cor Hydrotest Conducted Ind No
Preparer Name A** M****
Preparer Title Pipeline Safety And Compliance Advisor
Preparer Email A*****@s*******.com
Preparer Telephone 909-919-0463
Authorizer Name A** M****
Authorizer Title Pipeline Safety And Compliance Advisor
Authorizer Telephone 909-919-0463
Authorizer Email A*****@s*******.com
Narrative On 01/13/2020, socalgas was notified of a gas leak at 642 s alvarado street, los angeles. Socalgas crews were sent to the scene to perform leak investigation and centered leak over an 8-inch steel main. The leak was isolated by operating two mainline valves and gas was controlled at 05:25 on 01/14/2020. The leak was permanently repaired on 01/14/2020 by welding on a weld patch. All customer restores were completed on 01/15/2020. There were no injuries or further damages resulting from the release of gas. Further investigation shows the cause of leak was corrosion on bottom of main. A cathodic protection mitigation plan was developed to monitor the bell hole location until further remediation is determined. This incident was reported to DOT and cpuc due to gas release and damages exceeding $50,000. For any further questions, please contact ali matin at (909) 919-0463.

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