GD incident on 2019-12-06 — FL

Operator
Peoples Gas System Inc
Cause
Notification Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$83,388
Incident datetime
2019-12-06 12:59
Report number
Location
FL, DADE-BROWARD
Narrative
Contractor, jm power, struck a 6" pe main while boring under a canal. Jm power did not submit an underwater ticket as required by fs chapter 556; therefore, the canal was not marked with buoys. Two 2" bypasses were built to continue gas flow, 6 inch pipe was squeezed after. Crews, verified no pressure drops after bypass was installed. To make final repairs, a piece of 4" pe was inserted into the damaged area. 6" x 4" reducers were installed on either side of the inserted pipe. Cost information is does not include restoration (which should bring the costs to over $50k); will update with a supplemental when final costs are received. Supplemental created: added totals of restoration and additional contractor charges.. Costs are final.
Detailed record list
Occurred At
2019-12-06 12:59:00
Year
2019
Report Received Date
2020-01-15 00:00:00
Iyear
2019.0
Report Number
20200009.0
Supplemental Number
33450.0
Report Type
Supplemental Final
Operator Id
Name
Peoples Gas System Inc
Operator Street Address
Po Box 2562
Operator City Name
Tampa
Operator State Abbreviation
FL
Operator Postal Code
33601
Local Datetime
2019-12-06 12:59:00
Location Street Address
1194 University Dr
Location City Name
Coral Springs
Location County Name
Dade-Broward
Location State Abbreviation
FL
Location Postal Code
33071
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-12-10 21:36:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
635.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-12-06 12:59:00
On Site Datetime
2019-12-06 13:21:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Under A Water Canal
Depth Of Cover
300.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2002.0
Pipe Diameter
6.0
Pipe Specification
Sdr 11.5
Pipe Manufacturer
Plexco
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
83388.0
Est Cost Emergency
8870.0
Est Cost Other
648.0
Est Cost Other Details
Equipment Charges
Est Cost Unintentional Release
5541.0
Prpty
98447.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Damage was due to excavation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
Other
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
No
Service Interruption
No
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
S***** P****
Preparer Title
Supervisor Quality Assurance
Preparer Email
S******@t*********.com
Preparer Telephone
813-275-3730
Authorizer Name
S***** P****
Authorizer Title
Supervisor Quality Assurance
Authorizer Telephone
813-275-3730
Authorizer Email
S******@t*********.com
Narrative
Contractor, jm power, struck a 6" pe main while boring under a canal. Jm power did not submit an underwater ticket as required by fs chapter 556; therefore, the canal was not marked with buoys. Two 2" bypasses were built to continue gas flow, 6 inch pipe was squeezed after. Crews, verified no pressure drops after bypass was installed. To make final repairs, a piece of 4" pe was inserted into the damaged area. 6" x 4" reducers were installed on either side of the inserted pipe. Cost information is does not include restoration (which should bring the costs to over $50k); will update with a supplemental when final costs are received. Supplemental created: added totals of restoration and additional contractor charges.. Costs are final.
Occurred At 2019-12-06 12:59:00
Year 2019
Report Received Date 2020-01-15 00:00:00
Iyear 2019.0
Report Number 20200009.0
Supplemental Number 33450.0
Report Type Supplemental Final
Operator Id 15348 PHMSA Enforcement
Name Peoples Gas System Inc
Operator Street Address Po Box 2562
Operator City Name Tampa
Operator State Abbreviation FL
Operator Postal Code 33601
Local Datetime 2019-12-06 12:59:00
Location Street Address 1194 University Dr
Location City Name Coral Springs
Location County Name Dade-Broward
Location State Abbreviation FL
Location Postal Code 33071
Location Latitude 26.2459503 Google Maps OpenStreetMap
Location Longitude -80.2533146 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-12-10 21:36:00
Nrc Rpt Num 1266059 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 635.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-12-06 12:59:00
On Site Datetime 2019-12-06 13:21:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Under A Water Canal
Depth Of Cover 300.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2002.0
Pipe Diameter 6.0
Pipe Specification Sdr 11.5
Pipe Manufacturer Plexco
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 83388.0
Est Cost Emergency 8870.0
Est Cost Other 648.0
Est Cost Other Details Equipment Charges
Est Cost Unintentional Release 5541.0
Prpty 98447.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Damage was due to excavation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype Other
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Telecommunications
One Call Notified Ind No
Service Interruption No
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name S***** P****
Preparer Title Supervisor Quality Assurance
Preparer Email S******@t*********.com
Preparer Telephone 813-275-3730
Authorizer Name S***** P****
Authorizer Title Supervisor Quality Assurance
Authorizer Telephone 813-275-3730
Authorizer Email S******@t*********.com
Narrative Contractor, jm power, struck a 6" pe main while boring under a canal. Jm power did not submit an underwater ticket as required by fs chapter 556; therefore, the canal was not marked with buoys. Two 2" bypasses were built to continue gas flow, 6 inch pipe was squeezed after. Crews, verified no pressure drops after bypass was installed. To make final repairs, a piece of 4" pe was inserted into the damaged area. 6" x 4" reducers were installed on either side of the inserted pipe. Cost information is does not include restoration (which should bring the costs to over $50k); will update with a supplemental when final costs are received. Supplemental created: added totals of restoration and additional contractor charges.. Costs are final.

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