HL incident on 2019-12-17 — TX

Operator
Bkep Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-12-17 16:00
Report number
Location
TX
Narrative
Action environmental was on site to conduct routine tank roof cleaning. An action employee inadvertently opened the 2" water draw valve on the tank thinking it was the roof drain. Action was in the process of cleaning dirt and debris from the tank drain and the employee intended to open the roof drain but opened the wrong valve. The valve released 1-2 bbls of crude oil onto the ground. The cleanup was handled by action at their expense under the direction of bkep employees.
Detailed record list
Report Received Date
2019-12-20 00:00:00
Iyear
2019
Report Number
20190394
Supplemental Number
36349
Report Type
Supplemental Final
Operator Id
Name
Bkep Pipeline, Llc
Operator Street Address
2277 Plaza Drive Suite 500
Operator City Name
Sugar Land
Operator State Abbreviation
TX
Operator Postal Code
77479
Local Datetime
2019-12-17 16:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Recovered Bbls
1.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-12-17 16:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
On Site Datetime
2019-12-17 16:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Terminal
Segment Name
Tank 2509
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Not Within A Municipality
Onshore County Name
Payne
Designated Location
Milepost
Designated Name
Cushing Term
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Contractor Opened The Wrong Valve Releasing Oil From The Tank.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
3000
Est Cost Environmental
3080
Est Cost Other
0
Prpty
6080
Accident Psig
10
Mop Psig
10
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Caused by the actions of a contractor
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Preparer Name
R** M*****
Preparer Title
Sr Safety Engineer
Preparer Email
R*******@c********.com
Preparer Telephone
6209880317
Prepared Date
2022-02-16 00:00:00
Authorizer Name
K**** K****
Authorizer Telephone
6208708426
Authorizer Title
Vp Pipelines
Authorizer Email
K******@c********.com
Narrative
Action environmental was on site to conduct routine tank roof cleaning. An action employee inadvertently opened the 2" water draw valve on the tank thinking it was the roof drain. Action was in the process of cleaning dirt and debris from the tank drain and the employee intended to open the roof drain but opened the wrong valve. The valve released 1-2 bbls of crude oil onto the ground. The cleanup was handled by action at their expense under the direction of bkep employees.
Report Received Date 2019-12-20 00:00:00
Iyear 2019
Report Number 20190394
Supplemental Number 36349
Report Type Supplemental Final
Operator Id 32551 PHMSA Enforcement
Name Bkep Pipeline, Llc
Operator Street Address 2277 Plaza Drive Suite 500
Operator City Name Sugar Land
Operator State Abbreviation TX
Operator Postal Code 77479
Local Datetime 2019-12-17 16:00:00
Location Latitude 36.00512 Google Maps OpenStreetMap
Location Longitude -96.75145 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Recovered Bbls 1.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-12-17 16:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
On Site Datetime 2019-12-17 16:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Terminal
Segment Name Tank 2509
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Not Within A Municipality
Onshore County Name Payne
Designated Location Milepost
Designated Name Cushing Term
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Contractor Opened The Wrong Valve Releasing Oil From The Tank.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 3000
Est Cost Environmental 3080
Est Cost Other 0
Prpty 6080
Accident Psig 10
Mop Psig 10
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Caused by the actions of a contractor
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind No
Preparer Name R** M*****
Preparer Title Sr Safety Engineer
Preparer Email R*******@c********.com
Preparer Telephone 6209880317
Prepared Date 2022-02-16 00:00:00
Authorizer Name K**** K****
Authorizer Telephone 6208708426
Authorizer Title Vp Pipelines
Authorizer Email K******@c********.com
Narrative Action environmental was on site to conduct routine tank roof cleaning. An action employee inadvertently opened the 2" water draw valve on the tank thinking it was the roof drain. Action was in the process of cleaning dirt and debris from the tank drain and the employee intended to open the roof drain but opened the wrong valve. The valve released 1-2 bbls of crude oil onto the ground. The cleanup was handled by action at their expense under the direction of bkep employees.

All rights reserved. Copyright © by ClearPHMSA