HL incident on 2019-12-02 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20
Incident datetime
2019-12-02 11:30
Report number
Location
OK
Narrative
While performing a facility inspection, local operations personnel detected gasoline odors. Upon further inspection, a small release was observed originating from the thermal relief isolation valve on the prover drain line. Valves were closed to isolated the release and appropriate clean up activities were initiated. The release originated from the valve body seam on a two-piece 1/2" wog ball valve. The defective valve was replaced with a solid one-piece valve. The facility is being inspected to identify similar two-piece valves. The end plug and valve body are connected by threads. Results of the failure analysis indicate the seal at the interface between the end plug and valve body was damaged, likely from improper installation or overtightening. Supplemental (01/03/2020) part e 5f supplemental/final (02/12/2020) updated c-6, g6, g6-6, h
Detailed record list
Report Received Date
2019-12-19 00:00:00
Iyear
2019
Report Number
20190391
Supplemental Number
33321
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2019-12-02 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-12-02 11:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Location Was Isolated
On Site Datetime
2019-12-02 11:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cheyenne
Segment Name
Term No 419
Onshore State Abbreviation
Wy
Onshore Postal Code
82007
Onshore City Name
Not Within A Municipality
Onshore County Name
Laramie
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
20
Est Cost Emergency
200
Est Cost Environmental
200
Est Cost Other
0
Prpty
440
Accident Psig
25
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The drain line leak occurred in the facility which was not detected by mainline monitoring operation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Improper Assembly By Valve Manufacturer
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-02-12 00:00:00
Authorizer Name
B**** W****
Authorizer Telephone
918-574-7792
Authorizer Title
Mgr Integrity Mgmt And Regulatory Comp
Authorizer Email
B**********@m*********.com
Narrative
While performing a facility inspection, local operations personnel detected gasoline odors. Upon further inspection, a small release was observed originating from the thermal relief isolation valve on the prover drain line. Valves were closed to isolated the release and appropriate clean up activities were initiated. The release originated from the valve body seam on a two-piece 1/2" wog ball valve. The defective valve was replaced with a solid one-piece valve. The facility is being inspected to identify similar two-piece valves. The end plug and valve body are connected by threads. Results of the failure analysis indicate the seal at the interface between the end plug and valve body was damaged, likely from improper installation or overtightening. Supplemental (01/03/2020) part e 5f supplemental/final (02/12/2020) updated c-6, g6, g6-6, h
Report Received Date 2019-12-19 00:00:00
Iyear 2019
Report Number 20190391
Supplemental Number 33321
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2019-12-02 11:30:00
Location Latitude 41.10698 Google Maps OpenStreetMap
Location Longitude -104.832188 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-12-02 11:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Location Was Isolated
On Site Datetime 2019-12-02 11:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cheyenne
Segment Name Term No 419
Onshore State Abbreviation Wy
Onshore Postal Code 82007
Onshore City Name Not Within A Municipality
Onshore County Name Laramie
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 20
Est Cost Emergency 200
Est Cost Environmental 200
Est Cost Other 0
Prpty 440
Accident Psig 25
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The drain line leak occurred in the facility which was not detected by mainline monitoring operation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Improper Assembly By Valve Manufacturer
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2020-02-12 00:00:00
Authorizer Name B**** W****
Authorizer Telephone 918-574-7792
Authorizer Title Mgr Integrity Mgmt And Regulatory Comp
Authorizer Email B**********@m*********.com
Narrative While performing a facility inspection, local operations personnel detected gasoline odors. Upon further inspection, a small release was observed originating from the thermal relief isolation valve on the prover drain line. Valves were closed to isolated the release and appropriate clean up activities were initiated. The release originated from the valve body seam on a two-piece 1/2" wog ball valve. The defective valve was replaced with a solid one-piece valve. The facility is being inspected to identify similar two-piece valves. The end plug and valve body are connected by threads. Results of the failure analysis indicate the seal at the interface between the end plug and valve body was damaged, likely from improper installation or overtightening. Supplemental (01/03/2020) part e 5f supplemental/final (02/12/2020) updated c-6, g6, g6-6, h

All rights reserved. Copyright © by ClearPHMSA