HL incident on 2019-11-21 — PA

Operator
Buckeye Partners, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$70,000
Incident datetime
2019-11-21 16:00
Report number
Location
PA
Narrative
On november 21, 2019 at approximately 1600 hours, buckeye personnel were in progress of repairing an anomaly identified on a routine metal loss and ili assessment. During excavation of the anomaly a small weep was discovered on the topside of the pipe. The weep totaled less than one ounce of jet fuel and never made contact with the ground or soil. The product was cleaned up, the pipe segment was repaired. Repairs and excavation was complete by november 22, 2019 and the pipeline was restored to full operation by end of day november 23, 2019. An src report was submitted to PHMSA as a result of the routine imp assessment on november 19, 2019 under wms activity 19-168295. This report is being submitted based on cost of repair of the anomaly where the small weep was located and does not meet product release amount thresholds.
Detailed record list
Report Received Date
2019-12-19 00:00:00
Iyear
2019
Report Number
20190388
Supplemental Number
33164
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2019-11-21 16:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-11-21 16:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Active At The Time
On Site Datetime
2019-11-21 16:00:00
Nrc Rpt Datetime
2019-11-22 13:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Line 602
Segment Name
Line 602
Onshore State Abbreviation
Ny
Onshore Postal Code
11207
Onshore City Name
Brooklyn
Onshore County Name
Kings County
Designated Location
Milepost/valve Station
Designated Name
1173+32
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
168
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
60000
Pipe Specification
Api 5l, X60, 12.75
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Installation Year
1965
Manufactured Year
1965
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
70000
Est Cost Emergency
130000
Est Cost Environmental
0
Est Cost Other
10000
Est Cost Other Details
A Routine Ili Repair Was In Progress When Weep Was Discovered.
Prpty
210000
Accident Psig
0.25
Mop Psig
954
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Length Segment Isolated
Unknown
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was not active at the time of the incident and pressure in the pipe was drained down due to field work
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2019
Prior Damage
No
Collected Data Ind
Yes
Geometry Deformation Ind
Yes
Geometry Recent Year
2019
Other Recent Year
2019
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr
2019
Non Destructive Exam Ind
No
Preparer Name
D*** C*****
Preparer Title
District Compliance Specialist
Preparer Email
D******@b******.com
Preparer Telephone
484-707-1426
Prepared Date
2020-01-08 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On november 21, 2019 at approximately 1600 hours, buckeye personnel were in progress of repairing an anomaly identified on a routine metal loss and ili assessment. During excavation of the anomaly a small weep was discovered on the topside of the pipe. The weep totaled less than one ounce of jet fuel and never made contact with the ground or soil. The product was cleaned up, the pipe segment was repaired. Repairs and excavation was complete by november 22, 2019 and the pipeline was restored to full operation by end of day november 23, 2019. An src report was submitted to PHMSA as a result of the routine imp assessment on november 19, 2019 under wms activity 19-168295. This report is being submitted based on cost of repair of the anomaly where the small weep was located and does not meet product release amount thresholds.
Report Received Date 2019-12-19 00:00:00
Iyear 2019
Report Number 20190388
Supplemental Number 33164
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2019-11-21 16:00:00
Location Latitude 40.65778 Google Maps OpenStreetMap
Location Longitude -73.89545 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-11-21 16:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Not Active At The Time
On Site Datetime 2019-11-21 16:00:00
Nrc Rpt Datetime 2019-11-22 13:00:00
Nrc Rpt Num 1264845 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Line 602
Segment Name Line 602
Onshore State Abbreviation Ny
Onshore Postal Code 11207
Onshore City Name Brooklyn
Onshore County Name Kings County
Designated Location Milepost/valve Station
Designated Name 1173+32
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 168
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.25
Pipe Smys 60000
Pipe Specification Api 5l, X60, 12.75
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Installation Year 1965
Manufactured Year 1965
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 70000
Est Cost Emergency 130000
Est Cost Environmental 0
Est Cost Other 10000
Est Cost Other Details A Routine Ili Repair Was In Progress When Weep Was Discovered.
Prpty 210000
Accident Psig 0.25
Mop Psig 954
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Length Segment Isolated Unknown
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was not active at the time of the incident and pressure in the pipe was drained down due to field work
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2019
Prior Damage No
Collected Data Ind Yes
Geometry Deformation Ind Yes
Geometry Recent Year 2019
Other Recent Year 2019
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr 2019
Non Destructive Exam Ind No
Preparer Name D*** C*****
Preparer Title District Compliance Specialist
Preparer Email D******@b******.com
Preparer Telephone 484-707-1426
Prepared Date 2020-01-08 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On november 21, 2019 at approximately 1600 hours, buckeye personnel were in progress of repairing an anomaly identified on a routine metal loss and ili assessment. During excavation of the anomaly a small weep was discovered on the topside of the pipe. The weep totaled less than one ounce of jet fuel and never made contact with the ground or soil. The product was cleaned up, the pipe segment was repaired. Repairs and excavation was complete by november 22, 2019 and the pipeline was restored to full operation by end of day november 23, 2019. An src report was submitted to PHMSA as a result of the routine imp assessment on november 19, 2019 under wms activity 19-168295. This report is being submitted based on cost of repair of the anomaly where the small weep was located and does not meet product release amount thresholds.

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