HL incident on 2019-11-23 — TX

Operator
Sunoco Partners Marketing & Terminals Lp
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-11-23 21:30
Report number
Location
TX
Narrative
On 11/23/19 at approximately 17:30 an operator was switching the facility lineup from an inbound stream from one tank to another and a valve was incorrectly closed out of sequence causing an overpressure along several manifolds. Affected areas were visually inspected. At 21:30 pm it was discovered that approximately 15 barrels of crude had been released from failed valve gaskets at the texoma manifold caused by the overpressure event. The manifold was bypassed while emergency response and cleanup efforts were undertaken. All product was cleaned up and contaminated soil/rock were removed for on-site remediation. The failed gaskets have were replaced and the manifold was inspected. It was determined that the operator had incorrectly sequenced the valve alignment resulting in the overpressure. The operators qualifications were suspended and retraining was administered to prevent future reoccurrence.
Detailed record list
Report Received Date
2019-12-18 00:00:00
Iyear
2019
Report Number
20190386
Supplemental Number
33098
Report Type
Original Final
Operator Id
Name
Sunoco Partners Marketing & Terminals Lp
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-11-23 21:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-23 21:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Manifold Was Isolated
On Site Datetime
2019-11-23 21:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Nederland Terminal
Segment Name
Texoma Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Manifold
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
0
Est Cost Emergency
10000
Est Cost Environmental
13500
Est Cost Other
0
Prpty
24500
Accident Psig
500
Mop Psig
150
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2019-12-18 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 11/23/19 at approximately 17:30 an operator was switching the facility lineup from an inbound stream from one tank to another and a valve was incorrectly closed out of sequence causing an overpressure along several manifolds. Affected areas were visually inspected. At 21:30 pm it was discovered that approximately 15 barrels of crude had been released from failed valve gaskets at the texoma manifold caused by the overpressure event. The manifold was bypassed while emergency response and cleanup efforts were undertaken. All product was cleaned up and contaminated soil/rock were removed for on-site remediation. The failed gaskets have were replaced and the manifold was inspected. It was determined that the operator had incorrectly sequenced the valve alignment resulting in the overpressure. The operators qualifications were suspended and retraining was administered to prevent future reoccurrence.
Report Received Date 2019-12-18 00:00:00
Iyear 2019
Report Number 20190386
Supplemental Number 33098
Report Type Original Final
Operator Id 39706 PHMSA Enforcement
Name Sunoco Partners Marketing & Terminals Lp
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-11-23 21:30:00
Location Latitude 29.997984 Google Maps OpenStreetMap
Location Longitude -93.990191 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-11-23 21:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Manifold Was Isolated
On Site Datetime 2019-11-23 21:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Nederland Terminal
Segment Name Texoma Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 77627
Onshore City Name Nederland
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Manifold
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 0
Est Cost Emergency 10000
Est Cost Environmental 13500
Est Cost Other 0
Prpty 24500
Accident Psig 500
Mop Psig 150
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2019-12-18 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 11/23/19 at approximately 17:30 an operator was switching the facility lineup from an inbound stream from one tank to another and a valve was incorrectly closed out of sequence causing an overpressure along several manifolds. Affected areas were visually inspected. At 21:30 pm it was discovered that approximately 15 barrels of crude had been released from failed valve gaskets at the texoma manifold caused by the overpressure event. The manifold was bypassed while emergency response and cleanup efforts were undertaken. All product was cleaned up and contaminated soil/rock were removed for on-site remediation. The failed gaskets have were replaced and the manifold was inspected. It was determined that the operator had incorrectly sequenced the valve alignment resulting in the overpressure. The operators qualifications were suspended and retraining was administered to prevent future reoccurrence.

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