HL incident on 2019-11-11 — TX

Operator
Bayou Bridge Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-11-11 07:25
Report number
Location
TX
Narrative
Techs arrived at st. Martinville station at approximately 7:25am on 11/11/19 to perform routine station check. Upon station entry a small diameter tubing connection failure on top of pump 2120 was discovered and crude was misting from this point. The personnel notified console 4 to shut the pump down. The personnel then isolated the pump and assessed the amount released. Approximately 1 barrel of crude was released. A third party was contacted to help with the cleanup efforts. The area was cleaned up and new soil and rock was brought in. The contaminated soil and rock was collected and hauled off for proper disposal. Upon further investigation the cause of the release was determined that the tubing fitting had be over tightened during construction earlier in 2019. This resulted in the sealing point of the fitting mushrooming out and combined with the vibrations of the pump the tubing cracked at the feral sealing point. Other small diameter tubing connections were checked in the station for similar circumstances.
Detailed record list
Report Received Date
2019-12-11 00:00:00
Iyear
2019
Report Number
20190374
Supplemental Number
33057
Report Type
Original Final
Operator Id
Name
Bayou Bridge Pipeline, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-11-11 07:25:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-11 07:25:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Bypassed The Pump
On Site Datetime
2019-11-11 07:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
St Martinville Station
Segment Name
Bayou Bridge
Onshore State Abbreviation
La
Onshore Postal Code
70582
Onshore City Name
St. Martinville
Onshore County Name
St. Martin
Designated Location
Milepost/valve Station
Designated Name
29
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
18295
Est Cost Other
0
Prpty
18855
Accident Psig
460
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
No
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2019-12-11 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
Techs arrived at st. Martinville station at approximately 7:25am on 11/11/19 to perform routine station check. Upon station entry a small diameter tubing connection failure on top of pump 2120 was discovered and crude was misting from this point. The personnel notified console 4 to shut the pump down. The personnel then isolated the pump and assessed the amount released. Approximately 1 barrel of crude was released. A third party was contacted to help with the cleanup efforts. The area was cleaned up and new soil and rock was brought in. The contaminated soil and rock was collected and hauled off for proper disposal. Upon further investigation the cause of the release was determined that the tubing fitting had be over tightened during construction earlier in 2019. This resulted in the sealing point of the fitting mushrooming out and combined with the vibrations of the pump the tubing cracked at the feral sealing point. Other small diameter tubing connections were checked in the station for similar circumstances.
Report Received Date 2019-12-11 00:00:00
Iyear 2019
Report Number 20190374
Supplemental Number 33057
Report Type Original Final
Operator Id 39462 PHMSA Enforcement
Name Bayou Bridge Pipeline, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-11-11 07:25:00
Location Latitude 30.10774 Google Maps OpenStreetMap
Location Longitude -91.79631 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-11-11 07:25:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Bypassed The Pump
On Site Datetime 2019-11-11 07:25:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name St Martinville Station
Segment Name Bayou Bridge
Onshore State Abbreviation La
Onshore Postal Code 70582
Onshore City Name St. Martinville
Onshore County Name St. Martin
Designated Location Milepost/valve Station
Designated Name 29
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Environmental 18295
Est Cost Other 0
Prpty 18855
Accident Psig 460
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Construction
Operator Qualification Ind No
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2019-12-11 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative Techs arrived at st. Martinville station at approximately 7:25am on 11/11/19 to perform routine station check. Upon station entry a small diameter tubing connection failure on top of pump 2120 was discovered and crude was misting from this point. The personnel notified console 4 to shut the pump down. The personnel then isolated the pump and assessed the amount released. Approximately 1 barrel of crude was released. A third party was contacted to help with the cleanup efforts. The area was cleaned up and new soil and rock was brought in. The contaminated soil and rock was collected and hauled off for proper disposal. Upon further investigation the cause of the release was determined that the tubing fitting had be over tightened during construction earlier in 2019. This resulted in the sealing point of the fitting mushrooming out and combined with the vibrations of the pump the tubing cracked at the feral sealing point. Other small diameter tubing connections were checked in the station for similar circumstances.

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