HL incident on 2019-11-11 — TX

Operator
Centurion Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-11-11 22:49
Report number
Location
TX
Narrative
On november 11, 2019, at approximately 10:49 pm, a connecting carrier employee reported a release to centurion pipeline company l.P. (cpl) on its delivery skid in cushing, oklahoma, in lincoln county, oklahoma. Cpl isolated the pipeline at 10:55 pm after confirming the release visually. Approximately 0.35 barrels of crude oil were released from the flanged connection on mov-974. All oil was recovered in soil which was remediated on site. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on november 12, 2019, has a reference number of 1248615. The root cause analysis of the failure has determined that during a hydrotest performed on september 18, 2019, the flange on valve mov-974 was not torqued to specification. The gasket has been replaced and the flange bolts torqued to specification. Due to the time differential between the completion of the hydrotest and the release the operator contractors performing the work were not drug or alcohol tested.
Detailed record list
Report Received Date
2019-12-10 00:00:00
Iyear
2019
Report Number
20190372
Supplemental Number
33051
Report Type
Original Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
5 Greenway Plaza, Suite 1600
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046-7570
Local Datetime
2019-11-11 22:49:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.35
Recovered Bbls
0.35
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Other (Notification From Connection Personnel)
Incident Identified Datetime
2019-11-11 22:49:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-11-11 22:55:00
Restart Datetime
2019-11-13 08:20:00
On Site Datetime
2019-11-11 22:55:00
Nrc Rpt Datetime
2019-11-11 23:34:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing To Teppco#1
Segment Name
Cushing To Teppco#1
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Lincoln
Designated Location
Milepost/valve Station
Designated Name
Delivery Skid
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
1000
Est Cost Other
0
Prpty
1030
Accident Psig
30
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No, volumes did not reach alarm threshold
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D**** N*****
Preparer Title
Senior Risk Engineer Advisor
Preparer Email
D***********@c**********.com
Preparer Telephone
346-803-2688
Prepared Date
2019-12-10 00:00:00
Authorizer Name
D**** M****
Authorizer Telephone
346-803-2680
Authorizer Title
Senior Pipeline Compliance Consultant
Authorizer Email
D**********@c**********.com
Narrative
On november 11, 2019, at approximately 10:49 pm, a connecting carrier employee reported a release to centurion pipeline company l.P. (cpl) on its delivery skid in cushing, oklahoma, in lincoln county, oklahoma. Cpl isolated the pipeline at 10:55 pm after confirming the release visually. Approximately 0.35 barrels of crude oil were released from the flanged connection on mov-974. All oil was recovered in soil which was remediated on site. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on november 12, 2019, has a reference number of 1248615. The root cause analysis of the failure has determined that during a hydrotest performed on september 18, 2019, the flange on valve mov-974 was not torqued to specification. The gasket has been replaced and the flange bolts torqued to specification. Due to the time differential between the completion of the hydrotest and the release the operator contractors performing the work were not drug or alcohol tested.
Report Received Date 2019-12-10 00:00:00
Iyear 2019
Report Number 20190372
Supplemental Number 33051
Report Type Original Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 5 Greenway Plaza, Suite 1600
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046-7570
Local Datetime 2019-11-11 22:49:00
Location Latitude 35.941115 Google Maps OpenStreetMap
Location Longitude -96.746936 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.35
Recovered Bbls 0.35
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Other (Notification From Connection Personnel)
Incident Identified Datetime 2019-11-11 22:49:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-11-11 22:55:00
Restart Datetime 2019-11-13 08:20:00
On Site Datetime 2019-11-11 22:55:00
Nrc Rpt Datetime 2019-11-11 23:34:00
Nrc Rpt Num 1263705 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing To Teppco#1
Segment Name Cushing To Teppco#1
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Lincoln
Designated Location Milepost/valve Station
Designated Name Delivery Skid
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 1000
Est Cost Other 0
Prpty 1030
Accident Psig 30
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No, volumes did not reach alarm threshold
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D**** N*****
Preparer Title Senior Risk Engineer Advisor
Preparer Email D***********@c**********.com
Preparer Telephone 346-803-2688
Prepared Date 2019-12-10 00:00:00
Authorizer Name D**** M****
Authorizer Telephone 346-803-2680
Authorizer Title Senior Pipeline Compliance Consultant
Authorizer Email D**********@c**********.com
Narrative On november 11, 2019, at approximately 10:49 pm, a connecting carrier employee reported a release to centurion pipeline company l.P. (cpl) on its delivery skid in cushing, oklahoma, in lincoln county, oklahoma. Cpl isolated the pipeline at 10:55 pm after confirming the release visually. Approximately 0.35 barrels of crude oil were released from the flanged connection on mov-974. All oil was recovered in soil which was remediated on site. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on november 12, 2019, has a reference number of 1248615. The root cause analysis of the failure has determined that during a hydrotest performed on september 18, 2019, the flange on valve mov-974 was not torqued to specification. The gasket has been replaced and the flange bolts torqued to specification. Due to the time differential between the completion of the hydrotest and the release the operator contractors performing the work were not drug or alcohol tested.

All rights reserved. Copyright © by ClearPHMSA