HL incident on 2019-11-18 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2019-11-18 15:55
Report number
Location
TX
Narrative
Operator employee was opening the pig launcher at the south andrews station on line c14. When opened the crude oil inside the launcher overflowed the catch basin and spilled 0.37 barrels of crude onto the ground. Oil was contained on site and was remediated. Investigation determined that sump level prevented all of the crude within the trap from draining properly.
Detailed record list
Report Received Date
2019-12-10 00:00:00
Iyear
2019
Report Number
20190371
Supplemental Number
33415
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-11-18 15:55:00
Location Latitude
Location Longitude
-102.5425325
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-18 15:55:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Only Affected Pig Launcher, Which Was Isolated At Time Of Release.
On Site Datetime
2019-11-18 15:55:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
C14
Segment Name
South Andrews Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79714
Onshore City Name
Andrews
Onshore County Name
Andrews
Designated Location
Milepost/valve Station
Designated Name
S Andrews
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
1994
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
1000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1020
Accident Psig
0
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
5
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room personnel did not contribute to release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Sump Level Prevented Trap From Draining Completely
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2020-03-05 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
713-381-5647
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
Operator employee was opening the pig launcher at the south andrews station on line c14. When opened the crude oil inside the launcher overflowed the catch basin and spilled 0.37 barrels of crude onto the ground. Oil was contained on site and was remediated. Investigation determined that sump level prevented all of the crude within the trap from draining properly.
Report Received Date 2019-12-10 00:00:00
Iyear 2019
Report Number 20190371
Supplemental Number 33415
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-11-18 15:55:00
Location Latitude 32.3003976 Google Maps OpenStreetMap
Location Longitude -102.5425325 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-11-18 15:55:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Only Affected Pig Launcher, Which Was Isolated At Time Of Release.
On Site Datetime 2019-11-18 15:55:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name C14
Segment Name South Andrews Station
Onshore State Abbreviation Tx
Onshore Postal Code 79714
Onshore City Name Andrews
Onshore County Name Andrews
Designated Location Milepost/valve Station
Designated Name S Andrews
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 1994
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 1000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1020
Accident Psig 0
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 5
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room personnel did not contribute to release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Sump Level Prevented Trap From Draining Completely
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D**** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2020-03-05 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 713-381-5647
Authorizer Title Pipeline Compliance Engineer
Authorizer Email D*******@e****.com
Narrative Operator employee was opening the pig launcher at the south andrews station on line c14. When opened the crude oil inside the launcher overflowed the catch basin and spilled 0.37 barrels of crude onto the ground. Oil was contained on site and was remediated. Investigation determined that sump level prevented all of the crude within the trap from draining properly.

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