HL incident on 2019-11-16 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-11-16 17:10
Report number
Location
OH
Narrative
On 11/16/19 at 17:10, mpl field personnel noticed diesel fuel in an open excavation inside of pasadena station near valve it4. There were no movements taking place through or near the valve, however the texas city - pasadena system was shut down as a precaution during the response. It4 had been recently installed on 10/30/19. Mpl field personnel noticed a release and discovered a drain plug on the bottom of it4 was not secure. An estimated 3.1 bbls of product had been released. The drain plug was tightened to correct the issue. Product and contaminated soil were cleaned up promptly. Updated and submitted final report 3/6/20. Volume released and recovered changed from 3.0 to 3.1 bbls.
Detailed record list
Report Received Date
2019-12-06 00:00:00
Iyear
2019
Report Number
20190367
Supplemental Number
33428
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2019-11-16 17:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
3.1
Recovered Bbls
3.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-16 17:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-11-16 17:35:00
Restart Datetime
2019-11-16 19:11:00
On Site Datetime
2019-11-16 17:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena Station
Segment Name
Facility Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
77503
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Loose Valve Drain Plug.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
232
Est Cost Prop Damage
0
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
1232
Accident Psig
170
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
No
Preparer Name
K*** S*********
Preparer Title
Hes Professional
Preparer Email
K***********@m****************.com
Preparer Telephone
4194213073
Prepared Date
2020-03-06 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194213712
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
On 11/16/19 at 17:10, mpl field personnel noticed diesel fuel in an open excavation inside of pasadena station near valve it4. There were no movements taking place through or near the valve, however the texas city - pasadena system was shut down as a precaution during the response. It4 had been recently installed on 10/30/19. Mpl field personnel noticed a release and discovered a drain plug on the bottom of it4 was not secure. An estimated 3.1 bbls of product had been released. The drain plug was tightened to correct the issue. Product and contaminated soil were cleaned up promptly. Updated and submitted final report 3/6/20. Volume released and recovered changed from 3.0 to 3.1 bbls.
Report Received Date 2019-12-06 00:00:00
Iyear 2019
Report Number 20190367
Supplemental Number 33428
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2019-11-16 17:10:00
Location Latitude 29.717218 Google Maps OpenStreetMap
Location Longitude -95.173258 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 3.1
Recovered Bbls 3.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-11-16 17:10:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-11-16 17:35:00
Restart Datetime 2019-11-16 19:11:00
On Site Datetime 2019-11-16 17:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena Station
Segment Name Facility Piping
Onshore State Abbreviation Tx
Onshore Postal Code 77503
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Loose Valve Drain Plug.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 232
Est Cost Prop Damage 0
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 1232
Accident Psig 170
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind No
Preparer Name K*** S*********
Preparer Title Hes Professional
Preparer Email K***********@m****************.com
Preparer Telephone 4194213073
Prepared Date 2020-03-06 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 4194213712
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative On 11/16/19 at 17:10, mpl field personnel noticed diesel fuel in an open excavation inside of pasadena station near valve it4. There were no movements taking place through or near the valve, however the texas city - pasadena system was shut down as a precaution during the response. It4 had been recently installed on 10/30/19. Mpl field personnel noticed a release and discovered a drain plug on the bottom of it4 was not secure. An estimated 3.1 bbls of product had been released. The drain plug was tightened to correct the issue. Product and contaminated soil were cleaned up promptly. Updated and submitted final report 3/6/20. Volume released and recovered changed from 3.0 to 3.1 bbls.

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