HL incident on 2019-11-04 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2019-11-04 13:30
Report number
Location
PA
Narrative
At approximately 13:30 on november 4, 2019, buckeye personnel identified that a crude leak had occurred on a thermal relief valve belonging to pp861hf in the northwest corner of buckeye texas processing. At the time of discovery, the pipeline was not actively transporting product. The release was quantified at 10 gallons based on the amount of product on the aboveground piping and in the soil. Internal notifications were made and the railroad commission of texas was contacted and notified of the release. When conducting a physical inspection of the thermal relief valve, it was discovered that the fitting associated with the thermal relief valve connection to the stainless steel tubing had a crack in the interior. The fitting was replaced.
Detailed record list
Report Received Date
2019-12-03 00:00:00
Iyear
2019
Report Number
20190363
Supplemental Number
33218
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2019-11-04 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.25
Recovered Bbls
0.25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-04 13:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Was Discovered After Transfer Was Made On Pipeline
On Site Datetime
2019-11-04 13:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Btp Facility
Segment Name
Pp861hf
Onshore State Abbreviation
Tx
Onshore Postal Code
78409
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Milepost/valve Station
Designated Name
Btp Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Relief Line And Relief Equipment
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Tubing
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
12
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
3000
Est Cost Other
0
Prpty
3112
Accident Psig
180
Mop Psig
270
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was not actively transporting product when the release was identified.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Installation Ind
Yes
Preparer Name
V****** G**************
Preparer Title
Process Safety Engineer
Preparer Email
V***************@b******.com
Preparer Telephone
361-792-3083
Prepared Date
2020-01-22 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4916
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
At approximately 13:30 on november 4, 2019, buckeye personnel identified that a crude leak had occurred on a thermal relief valve belonging to pp861hf in the northwest corner of buckeye texas processing. At the time of discovery, the pipeline was not actively transporting product. The release was quantified at 10 gallons based on the amount of product on the aboveground piping and in the soil. Internal notifications were made and the railroad commission of texas was contacted and notified of the release. When conducting a physical inspection of the thermal relief valve, it was discovered that the fitting associated with the thermal relief valve connection to the stainless steel tubing had a crack in the interior. The fitting was replaced.
Report Received Date 2019-12-03 00:00:00
Iyear 2019
Report Number 20190363
Supplemental Number 33218
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2019-11-04 13:30:00
Location Latitude 27.8189044 Google Maps OpenStreetMap
Location Longitude -97.5079139 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.25
Recovered Bbls 0.25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-11-04 13:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Was Discovered After Transfer Was Made On Pipeline
On Site Datetime 2019-11-04 13:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Btp Facility
Segment Name Pp861hf
Onshore State Abbreviation Tx
Onshore Postal Code 78409
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Milepost/valve Station
Designated Name Btp Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Relief Line And Relief Equipment
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Tubing
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 12
Est Cost Prop Damage 100
Est Cost Emergency 0
Est Cost Environmental 3000
Est Cost Other 0
Prpty 3112
Accident Psig 180
Mop Psig 270
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was not actively transporting product when the release was identified.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Installation Ind Yes
Preparer Name V****** G**************
Preparer Title Process Safety Engineer
Preparer Email V***************@b******.com
Preparer Telephone 361-792-3083
Prepared Date 2020-01-22 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4916
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative At approximately 13:30 on november 4, 2019, buckeye personnel identified that a crude leak had occurred on a thermal relief valve belonging to pp861hf in the northwest corner of buckeye texas processing. At the time of discovery, the pipeline was not actively transporting product. The release was quantified at 10 gallons based on the amount of product on the aboveground piping and in the soil. Internal notifications were made and the railroad commission of texas was contacted and notified of the release. When conducting a physical inspection of the thermal relief valve, it was discovered that the fitting associated with the thermal relief valve connection to the stainless steel tubing had a crack in the interior. The fitting was replaced.

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