HL incident on 2019-10-27 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2019-10-27 10:00
Report number
Location
OK
Narrative
October 27th, 2019, a third party notified oneok's pipeline control after observing vapors originating from a pipeline mainline valve location. Oneok field personnel arrived on site and found the leak originating from the top seal of the check valve. Oneok personnel were able to tighten the associated bolts and stop leak. Oneok intends to remove the failed check valve prior to the end of 2019. Oneok will then disassemble the valve in order to determine the cause of the release. Updated 2/6/2020 - paula gates rippe check valve was removed on dec. 27th, 2019. Oneok maintenance technicians disassembled the valve and performed an inspection to all the components. There are no visible defects or damage to the face of either the body or cap. The o-ring groove appeared to be clean and free of damage as well. Damage is evident on the o-ring at the point of the release. Erosion of the o-ring is visible at the point of the release. The entire circumference of o-ring also shows a crease, indicating the o-ring was possibly pinched during installation, which may have contributed to the failure. Corrected apparent cause in part g to improper installation.
Detailed record list
Report Received Date
2019-11-25 00:00:00
Iyear
2019
Report Number
20190354
Supplemental Number
33298
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2019-10-27 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.4
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2019-10-27 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Was Eliminated Without Shutting Down Pipeline
On Site Datetime
2019-10-27 11:35:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Valve Site 635-121
Segment Name
Panther Creek Pipeline 10635
Onshore State Abbreviation
Ok
Onshore Postal Code
74538
Onshore City Name
Not Within A Municipality
Onshore County Name
Coal
Designated Location
Milepost/valve Station
Designated Name
Valve Site
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Check
Valve Manufacturer
Wheatley
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
5
Est Cost Prop Damage
40000
Est Cost Emergency
250
Est Cost Environmental
0
Est Cost Other
0
Prpty
40255
Accident Psig
727
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
16850
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had taken place prior to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Installation Ind
Yes
Preparer Name
P**** G**** R****
Preparer Title
Dot Compliance Coordinator
Preparer Email
P***************@o****.com
Preparer Telephone
5803956238
Prepared Date
2020-02-06 00:00:00
Authorizer Name
W***** A****
Authorizer Telephone
918-591-5081
Authorizer Title
Vp Ngl Pipelines And Terminals
Authorizer Email
W***********@o****.com
Narrative
October 27th, 2019, a third party notified oneok's pipeline control after observing vapors originating from a pipeline mainline valve location. Oneok field personnel arrived on site and found the leak originating from the top seal of the check valve. Oneok personnel were able to tighten the associated bolts and stop leak. Oneok intends to remove the failed check valve prior to the end of 2019. Oneok will then disassemble the valve in order to determine the cause of the release. Updated 2/6/2020 - paula gates rippe check valve was removed on dec. 27th, 2019. Oneok maintenance technicians disassembled the valve and performed an inspection to all the components. There are no visible defects or damage to the face of either the body or cap. The o-ring groove appeared to be clean and free of damage as well. Damage is evident on the o-ring at the point of the release. Erosion of the o-ring is visible at the point of the release. The entire circumference of o-ring also shows a crease, indicating the o-ring was possibly pinched during installation, which may have contributed to the failure. Corrected apparent cause in part g to improper installation.
Report Received Date 2019-11-25 00:00:00
Iyear 2019
Report Number 20190354
Supplemental Number 33298
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2019-10-27 10:00:00
Location Latitude 34.65129 Google Maps OpenStreetMap
Location Longitude -96.23159 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.4
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2019-10-27 10:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak Was Eliminated Without Shutting Down Pipeline
On Site Datetime 2019-10-27 11:35:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Valve Site 635-121
Segment Name Panther Creek Pipeline 10635
Onshore State Abbreviation Ok
Onshore Postal Code 74538
Onshore City Name Not Within A Municipality
Onshore County Name Coal
Designated Location Milepost/valve Station
Designated Name Valve Site
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Check
Valve Manufacturer Wheatley
Installation Year 2019
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 5
Est Cost Prop Damage 40000
Est Cost Emergency 250
Est Cost Environmental 0
Est Cost Other 0
Prpty 40255
Accident Psig 727
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 16850
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had taken place prior to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Installation Ind Yes
Preparer Name P**** G**** R****
Preparer Title Dot Compliance Coordinator
Preparer Email P***************@o****.com
Preparer Telephone 5803956238
Prepared Date 2020-02-06 00:00:00
Authorizer Name W***** A****
Authorizer Telephone 918-591-5081
Authorizer Title Vp Ngl Pipelines And Terminals
Authorizer Email W***********@o****.com
Narrative October 27th, 2019, a third party notified oneok's pipeline control after observing vapors originating from a pipeline mainline valve location. Oneok field personnel arrived on site and found the leak originating from the top seal of the check valve. Oneok personnel were able to tighten the associated bolts and stop leak. Oneok intends to remove the failed check valve prior to the end of 2019. Oneok will then disassemble the valve in order to determine the cause of the release. Updated 2/6/2020 - paula gates rippe check valve was removed on dec. 27th, 2019. Oneok maintenance technicians disassembled the valve and performed an inspection to all the components. There are no visible defects or damage to the face of either the body or cap. The o-ring groove appeared to be clean and free of damage as well. Damage is evident on the o-ring at the point of the release. Erosion of the o-ring is visible at the point of the release. The entire circumference of o-ring also shows a crease, indicating the o-ring was possibly pinched during installation, which may have contributed to the failure. Corrected apparent cause in part g to improper installation.

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