Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2019-10-29 — TX
Operator
Rose Rock Midstream L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$23,676
Incident datetime
2019-10-29 07:20
Report number
Location
TX
Narrative
Rose rock employee arrived at hudson station to do a station check on the morning of 10/29/2019 at 7:00. He drove up to the pumps and noticed oil on the ground and contacted the control center and his supervisor to notify them of the release. The control center shut the pumps down and the rose rock employee performed a lock-out of the upstream and downstream valves to isolate the release. The release was contained on rose rock property and did not impact water.
Detailed record list
Report Received Date
2019-11-25 00:00:00
Iyear
2019
Report Number
20190353
Supplemental Number
33133
Report Type
Supplemental Final
Operator Id
31476
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-10-29 07:20:00
Location Latitude
38.09338
Location Longitude
-98.58172
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-29 07:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-10-29 07:20:00
Restart Datetime
2019-10-30 16:30:00
On Site Datetime
2019-10-29 07:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hudson Station
Segment Name
Station Piping
Onshore State Abbreviation
Ks
Onshore Postal Code
67578
Onshore City Name
Not Within A Municipality
Onshore County Name
Stafford
Designated Location
Milepost/valve Station
Designated Name
Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Pangan Group Chendu Iron And Steel Co
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2012
Manufactured Year
2004
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
235
Est Cost Prop Damage
23676
Est Cost Emergency
7056
Est Cost Environmental
5900
Est Cost Other
1000
Est Cost Other Details
Estimated $1000 For Microbial Corrosion Analysis.
Prpty
37867
Accident Psig
12
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Corrosion related leak on low pressure tank suction piping.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
L*** V******
Preparer Title
Compliance Manager
Preparer Email
L*******@s*******.com
Preparer Telephone
9185248109
Prepared Date
2019-12-30 00:00:00
Authorizer Name
D**** Y****
Authorizer Telephone
6202686004
Authorizer Title
District Manager
Authorizer Email
D******@s*******.com
Narrative
Rose rock employee arrived at hudson station to do a station check on the morning of 10/29/2019 at 7:00. He drove up to the pumps and noticed oil on the ground and contacted the control center and his supervisor to notify them of the release. The control center shut the pumps down and the rose rock employee performed a lock-out of the upstream and downstream valves to isolate the release. The release was contained on rose rock property and did not impact water.
| Report Received Date | 2019-11-25 00:00:00 |
|---|---|
| Iyear | 2019 |
| Report Number | 20190353 |
| Supplemental Number | 33133 |
| Report Type | Supplemental Final |
| Operator Id | 31476 PHMSA Enforcement |
| Name | Rose Rock Midstream L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2019-10-29 07:20:00 |
| Location Latitude | 38.09338 Google Maps OpenStreetMap |
| Location Longitude | -98.58172 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 5 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2019-10-29 07:20:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2019-10-29 07:20:00 |
| Restart Datetime | 2019-10-30 16:30:00 |
| On Site Datetime | 2019-10-29 07:20:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Hudson Station |
| Segment Name | Station Piping |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67578 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Stafford |
| Designated Location | Milepost/valve Station |
| Designated Name | Station |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 36 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.375 |
| Pipe Smys | 42000 |
| Pipe Specification | Api 5l |
| Pipe Seam Type | Seamless |
| Pipe Manufacturer | Pangan Group Chendu Iron And Steel Co |
| Pipe Coating Type | Fusion Bonded Epoxy(Fbe) |
| Installation Year | 2012 |
| Manufactured Year | 2004 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 235 |
| Est Cost Prop Damage | 23676 |
| Est Cost Emergency | 7056 |
| Est Cost Environmental | 5900 |
| Est Cost Other | 1000 |
| Est Cost Other Details | Estimated $1000 For Microbial Corrosion Analysis. |
| Prpty | 37867 |
| Accident Psig | 12 |
| Mop Psig | 285 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Corrosion related leak on low pressure tank suction piping. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Microbiological Ind | Yes |
| Int Field Exam Basis Ind | Yes |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | Yes |
| Corrosion Lining | No |
| Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
| Corrosion Coupons | Yes |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | L*** V****** |
| Preparer Title | Compliance Manager |
| Preparer Email | L*******@s*******.com |
| Preparer Telephone | 9185248109 |
| Prepared Date | 2019-12-30 00:00:00 |
| Authorizer Name | D**** Y**** |
| Authorizer Telephone | 6202686004 |
| Authorizer Title | District Manager |
| Authorizer Email | D******@s*******.com |
| Narrative | Rose rock employee arrived at hudson station to do a station check on the morning of 10/29/2019 at 7:00. He drove up to the pumps and noticed oil on the ground and contacted the control center and his supervisor to notify them of the release. The control center shut the pumps down and the rose rock employee performed a lock-out of the upstream and downstream valves to isolate the release. The release was contained on rose rock property and did not impact water. |
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