HL incident on 2019-07-15 — TX

Operator
Anadarko Petroleum Corp
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2019-07-15 17:23
Report number
Location
TX
Narrative
On july 15th 2019 at approximately 7:23 pm, we received a phone call from an individual reporting a spill. This person called the phone number on the pipeline marker. We dispatched personnel to the area and confirmed the leak at approximately 8:45pm. The first valve was closed at 9:00 pm and then the second and final valve was closed at 9:30pm. The area was deemed safe and we contacted our third party clean up crew to come out the following morning to initiate clean up. The next morning the emergency one call was initiated prior to digging. By 10:30am the one call's were cleared and clean up began. This appears to be a pin hole leak on a previously out of service pipeline, so some details requested in this report are not known. We are land-farming the remaining oil under the direction of the wydeq, and these efforts will continue for some time. After discussing with PHMSA's aid team, it was decided that we can count the oil which is being land-farmed under the direction of the wydeq as recovered (part a). Part e questions 2, 3 and 5f: established mop unknown, thus making the determination of exceeding mop and % of smys unknown. The 950 mop number in part e is based on the set point of the relief valve after discussing with PHMSA's aid team.
Detailed record list
Report Received Date
2019-11-22 00:00:00
Iyear
2019
Report Number
20190352
Supplemental Number
36203
Report Type
Supplemental Final
Operator Id
Name
Anadarko Petroleum Corp
Operator Street Address
9950 Woodloch Forest Dr Suite 2800
Operator City Name
The Woodlands
Operator State Abbreviation
TX
Operator Postal Code
77380
Local Datetime
2019-07-15 19:23:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2250
Recovered Bbls
2250
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2019-07-15 17:23:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-15 21:30:00
Still Shutdown Ind
Yes
On Site Datetime
2019-07-15 20:45:00
Nrc Rpt Datetime
2019-07-16 10:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Wamsutter
Segment Name
Trunkline C
Onshore State Abbreviation
Wy
Onshore Postal Code
82901
Onshore City Name
Not Within A Municipality
Onshore County Name
Sweetwater
Designated Location
Milepost/valve Station
Designated Name
A/c Tie In
Federal
Yes
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Installation Year
1962
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
112000
Est Cost Prop Damage
30000
Est Cost Emergency
400
Est Cost Environmental
100000
Est Cost Other
0
Est Cost Other Details
Ongoing Environmental Remediation Costs, Landfarming Remaining Oil
Prpty
242400
Accident Psig
300
Mop Psig
950
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
31680
Internal Inspection Ind
No
Diameter Change Ind
Yes
Unsuitable Mainline Ind
Yes
Tight Mitered Ind
Yes
Other Restrictions Ind
Yes
Extra Thick Wall Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Multiple Pipe Dimensions
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No contributing factors from incident review. Controllers cannot control valves or pressure on pipe.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
B******* M******
Preparer Title
Staff Hse Representative
Preparer Email
B***************@w***************.com
Preparer Telephone
7209296732
Prepared Date
2022-01-05 00:00:00
Authorizer Name
M*** M****
Authorizer Telephone
307-352-3305
Authorizer Title
Field Foreman
Authorizer Email
M*********@w***************.com
Narrative
On july 15th 2019 at approximately 7:23 pm, we received a phone call from an individual reporting a spill. This person called the phone number on the pipeline marker. We dispatched personnel to the area and confirmed the leak at approximately 8:45pm. The first valve was closed at 9:00 pm and then the second and final valve was closed at 9:30pm. The area was deemed safe and we contacted our third party clean up crew to come out the following morning to initiate clean up. The next morning the emergency one call was initiated prior to digging. By 10:30am the one call's were cleared and clean up began. This appears to be a pin hole leak on a previously out of service pipeline, so some details requested in this report are not known. We are land-farming the remaining oil under the direction of the wydeq, and these efforts will continue for some time. After discussing with PHMSA's aid team, it was decided that we can count the oil which is being land-farmed under the direction of the wydeq as recovered (part a). Part e questions 2, 3 and 5f: established mop unknown, thus making the determination of exceeding mop and % of smys unknown. The 950 mop number in part e is based on the set point of the relief valve after discussing with PHMSA's aid team.
Report Received Date 2019-11-22 00:00:00
Iyear 2019
Report Number 20190352
Supplemental Number 36203
Report Type Supplemental Final
Operator Id 473 PHMSA Enforcement
Name Anadarko Petroleum Corp
Operator Street Address 9950 Woodloch Forest Dr Suite 2800
Operator City Name The Woodlands
Operator State Abbreviation TX
Operator Postal Code 77380
Local Datetime 2019-07-15 19:23:00
Location Latitude 41.61568 Google Maps OpenStreetMap
Location Longitude -108.38449 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2250
Recovered Bbls 2250
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2019-07-15 17:23:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-15 21:30:00
Still Shutdown Ind Yes
On Site Datetime 2019-07-15 20:45:00
Nrc Rpt Datetime 2019-07-16 10:27:00
Nrc Rpt Num 1252130 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Wamsutter
Segment Name Trunkline C
Onshore State Abbreviation Wy
Onshore Postal Code 82901
Onshore City Name Not Within A Municipality
Onshore County Name Sweetwater
Designated Location Milepost/valve Station
Designated Name A/c Tie In
Federal Yes
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Installation Year 1962
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 112000
Est Cost Prop Damage 30000
Est Cost Emergency 400
Est Cost Environmental 100000
Est Cost Other 0
Est Cost Other Details Ongoing Environmental Remediation Costs, Landfarming Remaining Oil
Prpty 242400
Accident Psig 300
Mop Psig 950
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 31680
Internal Inspection Ind No
Diameter Change Ind Yes
Unsuitable Mainline Ind Yes
Tight Mitered Ind Yes
Other Restrictions Ind Yes
Extra Thick Wall Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Other Complications Ind Yes
Inspect Comp Details Multiple Pipe Dimensions
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No contributing factors from incident review. Controllers cannot control valves or pressure on pipe.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name B******* M******
Preparer Title Staff Hse Representative
Preparer Email B***************@w***************.com
Preparer Telephone 7209296732
Prepared Date 2022-01-05 00:00:00
Authorizer Name M*** M****
Authorizer Telephone 307-352-3305
Authorizer Title Field Foreman
Authorizer Email M*********@w***************.com
Narrative On july 15th 2019 at approximately 7:23 pm, we received a phone call from an individual reporting a spill. This person called the phone number on the pipeline marker. We dispatched personnel to the area and confirmed the leak at approximately 8:45pm. The first valve was closed at 9:00 pm and then the second and final valve was closed at 9:30pm. The area was deemed safe and we contacted our third party clean up crew to come out the following morning to initiate clean up. The next morning the emergency one call was initiated prior to digging. By 10:30am the one call's were cleared and clean up began. This appears to be a pin hole leak on a previously out of service pipeline, so some details requested in this report are not known. We are land-farming the remaining oil under the direction of the wydeq, and these efforts will continue for some time. After discussing with PHMSA's aid team, it was decided that we can count the oil which is being land-farmed under the direction of the wydeq as recovered (part a). Part e questions 2, 3 and 5f: established mop unknown, thus making the determination of exceeding mop and % of smys unknown. The 950 mop number in part e is based on the set point of the relief valve after discussing with PHMSA's aid team.

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