HL incident on 2019-10-23 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,887
Incident datetime
2019-10-23 04:30
Report number
Location
TX
Narrative
On october 23, 2019 at 04:30 cst, operations technicians performing ground patrol discovered that the mixer on tank 2219 located in the cushing central terminal was on fire and product had been released. The release of the product is estimated at approximately 3 barrels of crude oil, which was contained within the tank dike area. Clean-up efforts have been completed and contaminated soil has been properly disposed of. The nrc was notified on october 23, 2019 at 05:31 cst (#1261913) and the 48-hour update was made on october 24, 2019 at 16:18 cst (#1262093). Upon further investigation of the mixer, it was determined that a bearing failure subsequently led to a mechanical seal failure resulting in a release. The mixer is currently blinded off and being sent to the manufacturer for further analysis.
Detailed record list
Report Received Date
2019-11-22 00:00:00
Iyear
2019
Report Number
20190351
Supplemental Number
32976
Report Type
Original Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2019-10-23 04:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-23 04:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Already Shut Down Due To Loss Of Power
On Site Datetime
2019-10-23 04:30:00
Nrc Rpt Datetime
2019-10-23 05:31:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Central Terminal
Segment Name
Tank 2219 Mixer
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
152
Est Cost Prop Damage
1887
Est Cost Emergency
3240
Est Cost Environmental
500
Est Cost Other
0
Prpty
5779
Accident Psig
9.6
Mop Psig
18.1
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Mixer Seal
Eq Additional Other Ind
Yes
Eq Additional Other Details
Mixer Bearing Failure
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2019-11-22 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On october 23, 2019 at 04:30 cst, operations technicians performing ground patrol discovered that the mixer on tank 2219 located in the cushing central terminal was on fire and product had been released. The release of the product is estimated at approximately 3 barrels of crude oil, which was contained within the tank dike area. Clean-up efforts have been completed and contaminated soil has been properly disposed of. The nrc was notified on october 23, 2019 at 05:31 cst (#1261913) and the 48-hour update was made on october 24, 2019 at 16:18 cst (#1262093). Upon further investigation of the mixer, it was determined that a bearing failure subsequently led to a mechanical seal failure resulting in a release. The mixer is currently blinded off and being sent to the manufacturer for further analysis.
Report Received Date 2019-11-22 00:00:00
Iyear 2019
Report Number 20190351
Supplemental Number 32976
Report Type Original Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2019-10-23 04:30:00
Location Latitude 35.94723 Google Maps OpenStreetMap
Location Longitude -96.75571 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-10-23 04:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Was Already Shut Down Due To Loss Of Power
On Site Datetime 2019-10-23 04:30:00
Nrc Rpt Datetime 2019-10-23 05:31:00
Nrc Rpt Num 1261913 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Central Terminal
Segment Name Tank 2219 Mixer
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 152
Est Cost Prop Damage 1887
Est Cost Emergency 3240
Est Cost Environmental 500
Est Cost Other 0
Prpty 5779
Accident Psig 9.6
Mop Psig 18.1
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Mixer Seal
Eq Additional Other Ind Yes
Eq Additional Other Details Mixer Bearing Failure
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2019-11-22 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On october 23, 2019 at 04:30 cst, operations technicians performing ground patrol discovered that the mixer on tank 2219 located in the cushing central terminal was on fire and product had been released. The release of the product is estimated at approximately 3 barrels of crude oil, which was contained within the tank dike area. Clean-up efforts have been completed and contaminated soil has been properly disposed of. The nrc was notified on october 23, 2019 at 05:31 cst (#1261913) and the 48-hour update was made on october 24, 2019 at 16:18 cst (#1262093). Upon further investigation of the mixer, it was determined that a bearing failure subsequently led to a mechanical seal failure resulting in a release. The mixer is currently blinded off and being sent to the manufacturer for further analysis.

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