HL incident on 2019-11-01 — TX

Operator
Enterprise Products Operating Llc
Cause
Other Outside Force Damage
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$29,033
Incident datetime
2019-11-01 00:20
Report number
Location
TX
Narrative
A power outage at cowden station was reported on october 31, 2019 at 23:33 communications were lost at the mov #0014 mainline block valve. At 2350 a 3rd party notified houston control center of a fire near the block valve. Fire was extinguished at 0326 on november 1, 2019 with assistance from local fire department. Damages to the pressure transmitter line on the valve were sustained. The line was bypassed and the pipeline was safely started back up. Investigation determined that the leak came from a pin-hole on the pressure transmitter's tubing. The pin-hole was caused from the electrical fault currents on the pipeline after the power loss occurred. An investigation determined that the leak came from a pinhole on the pressure transmitter's tubing. A downed tree caused a power line to ground fault outside cowden station. The power line fault caused an electrical arc between tubing fittings, resulting in a pinhole leak in the pressure transmitter tubing. Initial nrc call was made november 1, 2019 at 01:35 nrc# 1262794. The 48 hour update was placed november 1 at 09:44 nrc #1262810.
Detailed record list
Report Received Date
2019-11-21 00:00:00
Iyear
2019
Report Number
20190350
Supplemental Number
33517
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-10-31 23:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
13
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Notified Houston Control Center
Incident Identified Datetime
2019-11-01 00:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-10-31 23:30:00
Restart Datetime
2019-11-01 12:00:00
On Site Datetime
2019-11-01 00:20:00
Nrc Rpt Datetime
2019-11-01 01:35:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
3
Pipe Fac Name
A1
Segment Name
Mov 0014
Onshore State Abbreviation
Pa
Onshore Postal Code
15057
Onshore City Name
Not Within A Municipality
Onshore County Name
Washington
Designated Location
Milepost/valve Station
Designated Name
21.66
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
209
Est Cost Prop Damage
29033
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
29242
Accident Psig
364
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
211200
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Electrical Arcing From Other Equipment Or Facility
Outside Force Type
Electrical Arcing From Other Equipment Or Facility
Preparer Name
Y******* B**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
Y***@e****.com
Preparer Telephone
713-381-5650
Prepared Date
2020-03-26 00:00:00
Authorizer Name
Y******* B**
Authorizer Telephone
713-906-8726
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
Y***@e****.com
Narrative
A power outage at cowden station was reported on october 31, 2019 at 23:33 communications were lost at the mov #0014 mainline block valve. At 2350 a 3rd party notified houston control center of a fire near the block valve. Fire was extinguished at 0326 on november 1, 2019 with assistance from local fire department. Damages to the pressure transmitter line on the valve were sustained. The line was bypassed and the pipeline was safely started back up. Investigation determined that the leak came from a pin-hole on the pressure transmitter's tubing. The pin-hole was caused from the electrical fault currents on the pipeline after the power loss occurred. An investigation determined that the leak came from a pinhole on the pressure transmitter's tubing. A downed tree caused a power line to ground fault outside cowden station. The power line fault caused an electrical arc between tubing fittings, resulting in a pinhole leak in the pressure transmitter tubing. Initial nrc call was made november 1, 2019 at 01:35 nrc# 1262794. The 48 hour update was placed november 1 at 09:44 nrc #1262810.
Report Received Date 2019-11-21 00:00:00
Iyear 2019
Report Number 20190350
Supplemental Number 33517
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-10-31 23:30:00
Location Latitude 40.3105 Google Maps OpenStreetMap
Location Longitude -80.2609 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 13
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Notified Houston Control Center
Incident Identified Datetime 2019-11-01 00:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-10-31 23:30:00
Restart Datetime 2019-11-01 12:00:00
On Site Datetime 2019-11-01 00:20:00
Nrc Rpt Datetime 2019-11-01 01:35:00
Nrc Rpt Num 1262794 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 3
Pipe Fac Name A1
Segment Name Mov 0014
Onshore State Abbreviation Pa
Onshore Postal Code 15057
Onshore City Name Not Within A Municipality
Onshore County Name Washington
Designated Location Milepost/valve Station
Designated Name 21.66
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 209
Est Cost Prop Damage 29033
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 29242
Accident Psig 364
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 211200
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Electrical Arcing From Other Equipment Or Facility
Outside Force Type Electrical Arcing From Other Equipment Or Facility
Preparer Name Y******* B**
Preparer Title Pipeline Compliance Engineer
Preparer Email Y***@e****.com
Preparer Telephone 713-381-5650
Prepared Date 2020-03-26 00:00:00
Authorizer Name Y******* B**
Authorizer Telephone 713-906-8726
Authorizer Title Pipeline Compliance Engineer
Authorizer Email Y***@e****.com
Narrative A power outage at cowden station was reported on october 31, 2019 at 23:33 communications were lost at the mov #0014 mainline block valve. At 2350 a 3rd party notified houston control center of a fire near the block valve. Fire was extinguished at 0326 on november 1, 2019 with assistance from local fire department. Damages to the pressure transmitter line on the valve were sustained. The line was bypassed and the pipeline was safely started back up. Investigation determined that the leak came from a pin-hole on the pressure transmitter's tubing. The pin-hole was caused from the electrical fault currents on the pipeline after the power loss occurred. An investigation determined that the leak came from a pinhole on the pressure transmitter's tubing. A downed tree caused a power line to ground fault outside cowden station. The power line fault caused an electrical arc between tubing fittings, resulting in a pinhole leak in the pressure transmitter tubing. Initial nrc call was made november 1, 2019 at 01:35 nrc# 1262794. The 48 hour update was placed november 1 at 09:44 nrc #1262810.

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