HL incident on 2019-10-27 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-10-27 09:30
Report number
Location
TX
Narrative
At approximately 09:30 on 10/27 an enterprise technician discovered a crude oil release while making rounds at the station. Approximately 1 barrel of product had been released from a 1" ball valve near tank 390-34. The tank was in the final steps of an API 653 inspection and repair. Tank had been isolated from common station piping by an 8" valve installed on 10/24 and locked in the closed position. The 8" valve did not seat correctly which allowed product from a common manifold to enter the tank's recirculation system. Correct valve alignment was implemented and API inspection was continued. The crude release was immediately remediated. Employee's oq's were suspended pending re-training, oq's were reinstated on 11/02/2019. After investigation, the recommendation for returning tanks back to service will include conducting walk downs of tank piping prior to reconnection of the tank line to an active station line. Rrc was notified at 10:36 on 10/27/20 nrc was notified at 10:26 on 10/27/20 (nrc# 1262299) nrc 48 hour was given on 10/29/20 (nrc# 1262475)
Detailed record list
Report Received Date
2019-11-18 00:00:00
Iyear
2019
Report Number
20190341
Supplemental Number
33799
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-10-27 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.07
Recovered Bbls
1.07
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-27 09:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Open Valve Responsible Was Closed
On Site Datetime
2019-10-27 09:30:00
Nrc Rpt Datetime
2019-10-27 10:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Enterprise Houston Ship Channel
Segment Name
Tank 390-34
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Tank 390-34
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Tank Type
Atmospheric
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Misaligned Valve
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
412732
Est Cost Environmental
0
Est Cost Other
0
Prpty
412782
Accident Psig
150
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room personnel not involved
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2020-05-26 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
713-381-5647
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
At approximately 09:30 on 10/27 an enterprise technician discovered a crude oil release while making rounds at the station. Approximately 1 barrel of product had been released from a 1" ball valve near tank 390-34. The tank was in the final steps of an API 653 inspection and repair. Tank had been isolated from common station piping by an 8" valve installed on 10/24 and locked in the closed position. The 8" valve did not seat correctly which allowed product from a common manifold to enter the tank's recirculation system. Correct valve alignment was implemented and API inspection was continued. The crude release was immediately remediated. Employee's oq's were suspended pending re-training, oq's were reinstated on 11/02/2019. After investigation, the recommendation for returning tanks back to service will include conducting walk downs of tank piping prior to reconnection of the tank line to an active station line. Rrc was notified at 10:36 on 10/27/20 nrc was notified at 10:26 on 10/27/20 (nrc# 1262299) nrc 48 hour was given on 10/29/20 (nrc# 1262475)
Report Received Date 2019-11-18 00:00:00
Iyear 2019
Report Number 20190341
Supplemental Number 33799
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-10-27 09:30:00
Location Latitude 29.7459 Google Maps OpenStreetMap
Location Longitude -95.1265 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.07
Recovered Bbls 1.07
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-10-27 09:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Open Valve Responsible Was Closed
On Site Datetime 2019-10-27 09:30:00
Nrc Rpt Datetime 2019-10-27 10:26:00
Nrc Rpt Num 1262299 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Enterprise Houston Ship Channel
Segment Name Tank 390-34
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Tank 390-34
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Tank Type Atmospheric
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Misaligned Valve
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 0
Est Cost Emergency 412732
Est Cost Environmental 0
Est Cost Other 0
Prpty 412782
Accident Psig 150
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room personnel not involved
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D**** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2020-05-26 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 713-381-5647
Authorizer Title Pipeline Compliance Engineer
Authorizer Email D*******@e****.com
Narrative At approximately 09:30 on 10/27 an enterprise technician discovered a crude oil release while making rounds at the station. Approximately 1 barrel of product had been released from a 1" ball valve near tank 390-34. The tank was in the final steps of an API 653 inspection and repair. Tank had been isolated from common station piping by an 8" valve installed on 10/24 and locked in the closed position. The 8" valve did not seat correctly which allowed product from a common manifold to enter the tank's recirculation system. Correct valve alignment was implemented and API inspection was continued. The crude release was immediately remediated. Employee's oq's were suspended pending re-training, oq's were reinstated on 11/02/2019. After investigation, the recommendation for returning tanks back to service will include conducting walk downs of tank piping prior to reconnection of the tank line to an active station line. Rrc was notified at 10:36 on 10/27/20 nrc was notified at 10:26 on 10/27/20 (nrc# 1262299) nrc 48 hour was given on 10/29/20 (nrc# 1262475)

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