HL incident on 2019-11-08 — OH

Operator
Tesoro Logistics Operations, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150
Incident datetime
2019-11-08 14:00
Report number
Location
OH
Narrative
While completing facility inspection, operator discovered crude oil spraying from the valve body on a 1-inch ball valve on the low pressure pump suction piping at johnsons corner south station. Station pumps were immediately shut down and pipeline segment was isolated in order to stop the leak. The operators drained down the section of piping and installed a new valve in place of the failed valve. The contaminated soil was placed in secondary containment, upon completion of sampling the contaminated soil will be disposed of to an appropriate facility. All product was contained on-site. There was no injuries, impact to water or wildlife. The spill amount is estimated to be 38 gallons.
Detailed record list
Report Received Date
2019-11-15 00:00:00
Iyear
2019
Report Number
20190340
Supplemental Number
33077
Report Type
Supplemental Final
Operator Id
Name
Tesoro Logistics Operations, Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2019-11-08 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.9
Recovered Bbls
0.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-11-08 14:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-11-08 14:00:00
Restart Datetime
2019-11-08 18:10:00
On Site Datetime
2019-11-08 14:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Tesoro High Plains Pipelines
Segment Name
Johnson Corner Station
Onshore State Abbreviation
Nd
Onshore Postal Code
58847
Onshore City Name
Not Within A Municipality
Onshore County Name
Mckenzie
Designated Location
Milepost/valve Station
Designated Name
Johnson Corne
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
56
Est Cost Prop Damage
150
Est Cost Emergency
5000
Est Cost Environmental
10800
Est Cost Other
0
Prpty
16006
Accident Psig
73
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
100
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
This Is Station Piping With A Pump Immediately Downstream.
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
See Above
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was not discovered by the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
1-Inch Ball Valve That Is Blinded On Downstream Side.
Additional Defect Ind
Yes
Preparer Name
J*** M*****
Preparer Title
Hes Professional
Preparer Email
J******@m****************.com
Preparer Telephone
651-458-2608
Prepared Date
2019-12-16 00:00:00
Authorizer Name
J******* M***
Authorizer Telephone
303-454-6683
Authorizer Title
Director
Authorizer Email
J****@m****************.com
Narrative
While completing facility inspection, operator discovered crude oil spraying from the valve body on a 1-inch ball valve on the low pressure pump suction piping at johnsons corner south station. Station pumps were immediately shut down and pipeline segment was isolated in order to stop the leak. The operators drained down the section of piping and installed a new valve in place of the failed valve. The contaminated soil was placed in secondary containment, upon completion of sampling the contaminated soil will be disposed of to an appropriate facility. All product was contained on-site. There was no injuries, impact to water or wildlife. The spill amount is estimated to be 38 gallons.
Report Received Date 2019-11-15 00:00:00
Iyear 2019
Report Number 20190340
Supplemental Number 33077
Report Type Supplemental Final
Operator Id 38933 PHMSA Enforcement
Name Tesoro Logistics Operations, Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2019-11-08 14:00:00
Location Latitude 47.803227 Google Maps OpenStreetMap
Location Longitude -102.878937 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.9
Recovered Bbls 0.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-11-08 14:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-11-08 14:00:00
Restart Datetime 2019-11-08 18:10:00
On Site Datetime 2019-11-08 14:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Tesoro High Plains Pipelines
Segment Name Johnson Corner Station
Onshore State Abbreviation Nd
Onshore Postal Code 58847
Onshore City Name Not Within A Municipality
Onshore County Name Mckenzie
Designated Location Milepost/valve Station
Designated Name Johnson Corne
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 56
Est Cost Prop Damage 150
Est Cost Emergency 5000
Est Cost Environmental 10800
Est Cost Other 0
Prpty 16006
Accident Psig 73
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 100
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details This Is Station Piping With A Pump Immediately Downstream.
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details See Above
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was not discovered by the control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details 1-Inch Ball Valve That Is Blinded On Downstream Side.
Additional Defect Ind Yes
Preparer Name J*** M*****
Preparer Title Hes Professional
Preparer Email J******@m****************.com
Preparer Telephone 651-458-2608
Prepared Date 2019-12-16 00:00:00
Authorizer Name J******* M***
Authorizer Telephone 303-454-6683
Authorizer Title Director
Authorizer Email J****@m****************.com
Narrative While completing facility inspection, operator discovered crude oil spraying from the valve body on a 1-inch ball valve on the low pressure pump suction piping at johnsons corner south station. Station pumps were immediately shut down and pipeline segment was isolated in order to stop the leak. The operators drained down the section of piping and installed a new valve in place of the failed valve. The contaminated soil was placed in secondary containment, upon completion of sampling the contaminated soil will be disposed of to an appropriate facility. All product was contained on-site. There was no injuries, impact to water or wildlife. The spill amount is estimated to be 38 gallons.

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