HL incident on 2019-10-18 — TX

Operator
Nustar Logistics, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,050
Incident datetime
2019-10-18 06:54
Report number
Location
TX
Narrative
While performing a routine facility inspection, nustar discovered a crude oil leak at its wichita falls terminal. The leak originated at a mechanical seal on the mixer attached to tank 120m-1. Approximately 30 gallons were contained within a catch pan below the mixer, and approximately 24 gallons reached the soil inside the secondary containment area. The mixer was replaced, and the failed seal was sent to a third party for analysis. Update - the seal leaked when the rotating face broke, caused by over torqueing of the seal. The cause of the seal over-torqueing was investigated and remains unknown. It is possible a misalignment of the mixer shaft occurred prior to the installation of the mixer, or during the subsequent operation of the mixer, and contributed to the seal failure.
Detailed record list
Report Received Date
2019-11-14 00:00:00
Iyear
2019
Report Number
20190338
Supplemental Number
33101
Report Type
Supplemental Final
Operator Id
Name
Nustar Logistics, L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2019-10-18 06:54:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.29
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-18 06:54:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Ocurred On Tank Mixer, Terminal Facility Remained In Service
On Site Datetime
2019-10-18 06:54:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
16p Wichita Falls - Mckee Pipeline System
Segment Name
Wichita Falls Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
76305
Onshore City Name
Not Within A Municipality
Onshore County Name
Wichita
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Carbon Rotating Seal Face
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
69
Est Cost Prop Damage
1050
Est Cost Emergency
0
Est Cost Environmental
22550
Est Cost Other
0
Prpty
23669
Accident Psig
9
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither controller action nor control room issues contributed to the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Tank Mixer Seal
Eq Additional Other Ind
Yes
Eq Additional Other Details
Over-Torqueing Of The Mechanical Seal
Preparer Name
R****** P****
Preparer Title
Pipeline Safety Supervisor
Preparer Email
R************@n***********.com
Preparer Telephone
3612499417
Preparer Fax
2109187117
Prepared Date
2019-12-18 00:00:00
Authorizer Name
J**** R********
Authorizer Telephone
8063711304
Authorizer Title
General Manager
Authorizer Email
J**************@n***********.com
Narrative
While performing a routine facility inspection, nustar discovered a crude oil leak at its wichita falls terminal. The leak originated at a mechanical seal on the mixer attached to tank 120m-1. Approximately 30 gallons were contained within a catch pan below the mixer, and approximately 24 gallons reached the soil inside the secondary containment area. The mixer was replaced, and the failed seal was sent to a third party for analysis. Update - the seal leaked when the rotating face broke, caused by over torqueing of the seal. The cause of the seal over-torqueing was investigated and remains unknown. It is possible a misalignment of the mixer shaft occurred prior to the installation of the mixer, or during the subsequent operation of the mixer, and contributed to the seal failure.
Report Received Date 2019-11-14 00:00:00
Iyear 2019
Report Number 20190338
Supplemental Number 33101
Report Type Supplemental Final
Operator Id 31454 PHMSA Enforcement
Name Nustar Logistics, L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2019-10-18 06:54:00
Location Latitude 33.91298 Google Maps OpenStreetMap
Location Longitude -98.43419 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.29
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-10-18 06:54:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak Ocurred On Tank Mixer, Terminal Facility Remained In Service
On Site Datetime 2019-10-18 06:54:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 16p Wichita Falls - Mckee Pipeline System
Segment Name Wichita Falls Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 76305
Onshore City Name Not Within A Municipality
Onshore County Name Wichita
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Carbon Rotating Seal Face
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 69
Est Cost Prop Damage 1050
Est Cost Emergency 0
Est Cost Environmental 22550
Est Cost Other 0
Prpty 23669
Accident Psig 9
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither controller action nor control room issues contributed to the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Tank Mixer Seal
Eq Additional Other Ind Yes
Eq Additional Other Details Over-Torqueing Of The Mechanical Seal
Preparer Name R****** P****
Preparer Title Pipeline Safety Supervisor
Preparer Email R************@n***********.com
Preparer Telephone 3612499417
Preparer Fax 2109187117
Prepared Date 2019-12-18 00:00:00
Authorizer Name J**** R********
Authorizer Telephone 8063711304
Authorizer Title General Manager
Authorizer Email J**************@n***********.com
Narrative While performing a routine facility inspection, nustar discovered a crude oil leak at its wichita falls terminal. The leak originated at a mechanical seal on the mixer attached to tank 120m-1. Approximately 30 gallons were contained within a catch pan below the mixer, and approximately 24 gallons reached the soil inside the secondary containment area. The mixer was replaced, and the failed seal was sent to a third party for analysis. Update - the seal leaked when the rotating face broke, caused by over torqueing of the seal. The cause of the seal over-torqueing was investigated and remains unknown. It is possible a misalignment of the mixer shaft occurred prior to the installation of the mixer, or during the subsequent operation of the mixer, and contributed to the seal failure.

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