HL incident on 2019-10-07 — TX

Operator
Nustar Logistics, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2019-10-07 16:44
Report number
Location
TX
Narrative
A leak was discovered inside nustar's corpus christi crude terminal by nustar operations personnel, who noticed an odor while working inside the facility. The leak originated at a below-grade 10-inch steel pipe that was designed to assist with the circulation of crude oil within tk 400m-1. The segment containing the leak was immediately isolated by nustar operations personnel using valves at an adjacent manifold on tk 400m-1. A section of pipe containing the leak has been removed and will be sent for analysis to determine the cause of failure. Update - the failure occurred due to through wall corrosion caused by corrosion cells associated with solids deposits on the pipe id. Stagnant conditions allowed solids and water to accumulated on the bottom of the pipe. Chlorine and sulfur were present as corrosion promoters.
Detailed record list
Report Received Date
2019-11-06 00:00:00
Iyear
2019
Report Number
20190334
Supplemental Number
33228
Report Type
Supplemental Final
Operator Id
Name
Nustar Logistics, L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2019-10-07 16:44:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
18.75
Recovered Bbls
18.75
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-07 16:44:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Booster Pumps Were Shut Down, Terminal Facility Remained In Operation
On Site Datetime
2019-10-07 16:44:00
Nrc Rpt Datetime
2019-10-07 17:41:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
45p Oakville Pipeline System
Segment Name
Corpus Christi North Beach Crude Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
78402
Onshore City Name
Not Within A Municipality
Onshore County Name
Nueces
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.365
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2012
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1004
Est Cost Prop Damage
15000
Est Cost Emergency
6089
Est Cost Environmental
55308
Est Cost Other
4667
Est Cost Other Details
Metallurgical Lab
Prpty
82068
Accident Psig
114
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither controller action nor control room issues contributed to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Corrosion Under Deposit
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R****** P****
Preparer Title
Pipeline Safety Supervisor
Preparer Email
R************@n***********.com
Preparer Telephone
361-249-9417
Preparer Fax
210-918-7007
Prepared Date
2020-01-23 00:00:00
Authorizer Name
W** G***
Authorizer Telephone
361-249-9402
Authorizer Title
Vice President And General Manager
Authorizer Email
W*******@n***********.com
Narrative
A leak was discovered inside nustar's corpus christi crude terminal by nustar operations personnel, who noticed an odor while working inside the facility. The leak originated at a below-grade 10-inch steel pipe that was designed to assist with the circulation of crude oil within tk 400m-1. The segment containing the leak was immediately isolated by nustar operations personnel using valves at an adjacent manifold on tk 400m-1. A section of pipe containing the leak has been removed and will be sent for analysis to determine the cause of failure. Update - the failure occurred due to through wall corrosion caused by corrosion cells associated with solids deposits on the pipe id. Stagnant conditions allowed solids and water to accumulated on the bottom of the pipe. Chlorine and sulfur were present as corrosion promoters.
Report Received Date 2019-11-06 00:00:00
Iyear 2019
Report Number 20190334
Supplemental Number 33228
Report Type Supplemental Final
Operator Id 31454 PHMSA Enforcement
Name Nustar Logistics, L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2019-10-07 16:44:00
Location Latitude 27.81748 Google Maps OpenStreetMap
Location Longitude -97.40699 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 18.75
Recovered Bbls 18.75
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-10-07 16:44:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Booster Pumps Were Shut Down, Terminal Facility Remained In Operation
On Site Datetime 2019-10-07 16:44:00
Nrc Rpt Datetime 2019-10-07 17:41:00
Nrc Rpt Num 1260511 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 45p Oakville Pipeline System
Segment Name Corpus Christi North Beach Crude Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 78402
Onshore City Name Not Within A Municipality
Onshore County Name Nueces
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.365
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2012
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1004
Est Cost Prop Damage 15000
Est Cost Emergency 6089
Est Cost Environmental 55308
Est Cost Other 4667
Est Cost Other Details Metallurgical Lab
Prpty 82068
Accident Psig 114
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither controller action nor control room issues contributed to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Corrosion Under Deposit
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R****** P****
Preparer Title Pipeline Safety Supervisor
Preparer Email R************@n***********.com
Preparer Telephone 361-249-9417
Preparer Fax 210-918-7007
Prepared Date 2020-01-23 00:00:00
Authorizer Name W** G***
Authorizer Telephone 361-249-9402
Authorizer Title Vice President And General Manager
Authorizer Email W*******@n***********.com
Narrative A leak was discovered inside nustar's corpus christi crude terminal by nustar operations personnel, who noticed an odor while working inside the facility. The leak originated at a below-grade 10-inch steel pipe that was designed to assist with the circulation of crude oil within tk 400m-1. The segment containing the leak was immediately isolated by nustar operations personnel using valves at an adjacent manifold on tk 400m-1. A section of pipe containing the leak has been removed and will be sent for analysis to determine the cause of failure. Update - the failure occurred due to through wall corrosion caused by corrosion cells associated with solids deposits on the pipe id. Stagnant conditions allowed solids and water to accumulated on the bottom of the pipe. Chlorine and sulfur were present as corrosion promoters.

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