HL incident on 2019-10-09 — CO

Operator
Western Refining Logistics, Lp
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-10-09 09:40
Report number
Location
CO
Narrative
On october 9, 2019, during a pig removal from the receiver operation, the barrel was being refilled to be put into operation. One of the barrel drain valves was not closed. The valve was not closed causing flow to go into the sump and over flow from the sump. The amount was determined to be 1.9 barrels onto the ground. 30 gallons were recovered and put back into sump. High level in the sump shut the 16" pipeline down. There were no injuries or fatalities. The product was contained entirely on the company property. The spill was promptly cleaned up.
Detailed record list
Report Received Date
2019-11-01 00:00:00
Iyear
2019
Report Number
20190330
Supplemental Number
32893
Report Type
Original Final
Operator Id
Name
Western Refining Logistics, Lp
Operator Street Address
1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80202
Local Datetime
2019-10-09 09:40:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.9
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-09 09:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-10-09 09:40:00
Restart Datetime
2019-10-09 17:00:00
On Site Datetime
2019-10-09 09:40:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Placitas Station
Segment Name
16 Inch Line
Onshore State Abbreviation
Nm
Onshore Postal Code
87043
Onshore City Name
Placitas Villlage
Onshore County Name
Sandoval
Designated Location
Milepost/valve Station
Designated Name
Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2007
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
2619
Est Cost Prop Damage
0
Est Cost Emergency
4185
Est Cost Environmental
602
Est Cost Other
0
Prpty
7406
Accident Psig
328
Mop Psig
784
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
6
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operators onsite had control of the pigging operation.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D*** R*******
Preparer Title
Hes Professional
Preparer Email
D*********@m****************.com
Preparer Telephone
5056324039
Prepared Date
2019-11-01 00:00:00
Authorizer Name
M*** B*****
Authorizer Telephone
6067392515
Authorizer Title
Safety Supervisor
Authorizer Email
M*******@m****************.com
Narrative
On october 9, 2019, during a pig removal from the receiver operation, the barrel was being refilled to be put into operation. One of the barrel drain valves was not closed. The valve was not closed causing flow to go into the sump and over flow from the sump. The amount was determined to be 1.9 barrels onto the ground. 30 gallons were recovered and put back into sump. High level in the sump shut the 16" pipeline down. There were no injuries or fatalities. The product was contained entirely on the company property. The spill was promptly cleaned up.
Report Received Date 2019-11-01 00:00:00
Iyear 2019
Report Number 20190330
Supplemental Number 32893
Report Type Original Final
Operator Id 31574 PHMSA Enforcement
Name Western Refining Logistics, Lp
Operator Street Address 1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80202
Local Datetime 2019-10-09 09:40:00
Location Latitude 35.3191 Google Maps OpenStreetMap
Location Longitude -106.4336 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.9
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-10-09 09:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-10-09 09:40:00
Restart Datetime 2019-10-09 17:00:00
On Site Datetime 2019-10-09 09:40:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Placitas Station
Segment Name 16 Inch Line
Onshore State Abbreviation Nm
Onshore Postal Code 87043
Onshore City Name Placitas Villlage
Onshore County Name Sandoval
Designated Location Milepost/valve Station
Designated Name Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2007
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 2619
Est Cost Prop Damage 0
Est Cost Emergency 4185
Est Cost Environmental 602
Est Cost Other 0
Prpty 7406
Accident Psig 328
Mop Psig 784
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 6
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operators onsite had control of the pigging operation.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D*** R*******
Preparer Title Hes Professional
Preparer Email D*********@m****************.com
Preparer Telephone 5056324039
Prepared Date 2019-11-01 00:00:00
Authorizer Name M*** B*****
Authorizer Telephone 6067392515
Authorizer Title Safety Supervisor
Authorizer Email M*******@m****************.com
Narrative On october 9, 2019, during a pig removal from the receiver operation, the barrel was being refilled to be put into operation. One of the barrel drain valves was not closed. The valve was not closed causing flow to go into the sump and over flow from the sump. The amount was determined to be 1.9 barrels onto the ground. 30 gallons were recovered and put back into sump. High level in the sump shut the 16" pipeline down. There were no injuries or fatalities. The product was contained entirely on the company property. The spill was promptly cleaned up.

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