HL incident on 2019-10-02 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$118,336
Incident datetime
2019-10-02 14:00
Report number
Location
TX
Narrative
On october 2, 2019 at 14:00, an enterprise contractor discovered a gasoline leak near the meter skid 2177 at the beaumont terminal. It was discovered that the o-ring seal around a filter access door was leaking. Approximately 3 gallons of gasoline leaked on the ground. The leak was mitigated by isolating the meter skid area. During investigation of the leak, it was discovered that adequate thermal relief was not in place on the filters connected to the meter skid. The filters were disconnected from the meter and the pipeline was put back into the service. Permanent repairs were confirmed to exceed the $50,000 nrc threshold on october 15 at 10:30. Nrc call was made at 11:03 with incident #1261154. 48 hour update was made on october16 at 15:14 with incident #1261288. November 20, 2019 all required thermal relief was installed and the meter skid placed into service.
Detailed record list
Report Received Date
2019-10-31 00:00:00
Iyear
2019
Report Number
20190327
Supplemental Number
32975
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-10-02 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-10-02 14:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-10-02 14:00:00
Restart Datetime
2019-10-06 07:00:00
On Site Datetime
2019-10-02 14:00:00
Nrc Rpt Datetime
2019-10-15 10:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Terminal 2
Segment Name
Meter Skid 2177
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Mp 0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
118336
Est Cost Emergency
50
Est Cost Environmental
0
Est Cost Other
0
Prpty
118386
Accident Psig
829
Mop Psig
720
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The operator did not have any impact or determination of this leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related No Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
R***** B********
Preparer Title
Pipeline Compliance Specialist
Preparer Email
R**********@e****.com
Preparer Telephone
713-381-4611
Prepared Date
2019-11-22 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Compliance Manager
Authorizer Email
S******@e****.com
Narrative
On october 2, 2019 at 14:00, an enterprise contractor discovered a gasoline leak near the meter skid 2177 at the beaumont terminal. It was discovered that the o-ring seal around a filter access door was leaking. Approximately 3 gallons of gasoline leaked on the ground. The leak was mitigated by isolating the meter skid area. During investigation of the leak, it was discovered that adequate thermal relief was not in place on the filters connected to the meter skid. The filters were disconnected from the meter and the pipeline was put back into the service. Permanent repairs were confirmed to exceed the $50,000 nrc threshold on october 15 at 10:30. Nrc call was made at 11:03 with incident #1261154. 48 hour update was made on october16 at 15:14 with incident #1261288. November 20, 2019 all required thermal relief was installed and the meter skid placed into service.
Report Received Date 2019-10-31 00:00:00
Iyear 2019
Report Number 20190327
Supplemental Number 32975
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-10-02 14:00:00
Location Latitude 30.009092 Google Maps OpenStreetMap
Location Longitude -94.060381 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-10-02 14:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-10-02 14:00:00
Restart Datetime 2019-10-06 07:00:00
On Site Datetime 2019-10-02 14:00:00
Nrc Rpt Datetime 2019-10-15 10:03:00
Nrc Rpt Num 1261154 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Beaumont Terminal 2
Segment Name Meter Skid 2177
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Mp 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 118336
Est Cost Emergency 50
Est Cost Environmental 0
Est Cost Other 0
Prpty 118386
Accident Psig 829
Mop Psig 720
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The operator did not have any impact or determination of this leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related No Proc Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name R***** B********
Preparer Title Pipeline Compliance Specialist
Preparer Email R**********@e****.com
Preparer Telephone 713-381-4611
Prepared Date 2019-11-22 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Compliance Manager
Authorizer Email S******@e****.com
Narrative On october 2, 2019 at 14:00, an enterprise contractor discovered a gasoline leak near the meter skid 2177 at the beaumont terminal. It was discovered that the o-ring seal around a filter access door was leaking. Approximately 3 gallons of gasoline leaked on the ground. The leak was mitigated by isolating the meter skid area. During investigation of the leak, it was discovered that adequate thermal relief was not in place on the filters connected to the meter skid. The filters were disconnected from the meter and the pipeline was put back into the service. Permanent repairs were confirmed to exceed the $50,000 nrc threshold on october 15 at 10:30. Nrc call was made at 11:03 with incident #1261154. 48 hour update was made on october16 at 15:14 with incident #1261288. November 20, 2019 all required thermal relief was installed and the meter skid placed into service.

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