HL incident on 2019-10-01 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-10-01 11:50
Report number
Location
PA
Narrative
On 10/1/2019 at approximately 11:50 am local buckeye personnel was performing routine maintenance of 'cleaning strainer' when two barrels of gasoline began escaping from strainer opening. The local operators immediately closed and isolated the strainer. Upon investigation it was determined that local operations did not properly follow procedures to prepare the area for maintenance by turning off the power source and locking out the actuator. This allowed the controller to open an incorrect remote valve in error. All internal and external notifications were made. Osro arrived on site. Clean up activities continued for several days. All affected stone and soil was properly disposed of. All personnel were drug and alcohol tested. There were no injuries. No further remediation is needed.
Detailed record list
Report Received Date
2019-10-28 00:00:00
Iyear
2019
Report Number
20190324
Supplemental Number
32876
Report Type
Original Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2019-10-01 11:50:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-10-01 11:50:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Not Active - It Was Being Prepared To Start
On Site Datetime
2019-10-01 11:50:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Macungie Station
Segment Name
L620 Strainer
Onshore State Abbreviation
Pa
Onshore Postal Code
18062
Onshore City Name
Macungie
Onshore County Name
Lehigh
Designated Location
Milepost/valve Station
Designated Name
L620 Strainer
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Open Strainer
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
3910
Est Cost Environmental
22865
Est Cost Other
0
Prpty
26775
Accident Psig
371
Mop Psig
900
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest Incorrect Action Ind
Yes
Invest Incorrect Procedure Ind
Yes
Invest Maint Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
4
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Routine Maintenance Of 'cleaning Strainer' Was Being Performed. Local Operations Failed To Properly Turn Off Power And Secure The Valve Before Starting.
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D*** C*****
Preparer Title
District Compliance Specialist
Preparer Email
D******@b******.com
Preparer Telephone
484-707-1426
Prepared Date
2019-10-28 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Directory Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 10/1/2019 at approximately 11:50 am local buckeye personnel was performing routine maintenance of 'cleaning strainer' when two barrels of gasoline began escaping from strainer opening. The local operators immediately closed and isolated the strainer. Upon investigation it was determined that local operations did not properly follow procedures to prepare the area for maintenance by turning off the power source and locking out the actuator. This allowed the controller to open an incorrect remote valve in error. All internal and external notifications were made. Osro arrived on site. Clean up activities continued for several days. All affected stone and soil was properly disposed of. All personnel were drug and alcohol tested. There were no injuries. No further remediation is needed.
Report Received Date 2019-10-28 00:00:00
Iyear 2019
Report Number 20190324
Supplemental Number 32876
Report Type Original Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2019-10-01 11:50:00
Location Latitude 40.519305 Google Maps OpenStreetMap
Location Longitude -75.534154 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-10-01 11:50:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Not Active - It Was Being Prepared To Start
On Site Datetime 2019-10-01 11:50:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Macungie Station
Segment Name L620 Strainer
Onshore State Abbreviation Pa
Onshore Postal Code 18062
Onshore City Name Macungie
Onshore County Name Lehigh
Designated Location Milepost/valve Station
Designated Name L620 Strainer
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Open Strainer
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 3910
Est Cost Environmental 22865
Est Cost Other 0
Prpty 26775
Accident Psig 371
Mop Psig 900
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest Incorrect Action Ind Yes
Invest Incorrect Procedure Ind Yes
Invest Maint Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 4
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Routine Maintenance Of 'cleaning Strainer' Was Being Performed. Local Operations Failed To Properly Turn Off Power And Secure The Valve Before Starting.
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D*** C*****
Preparer Title District Compliance Specialist
Preparer Email D******@b******.com
Preparer Telephone 484-707-1426
Prepared Date 2019-10-28 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Directory Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 10/1/2019 at approximately 11:50 am local buckeye personnel was performing routine maintenance of 'cleaning strainer' when two barrels of gasoline began escaping from strainer opening. The local operators immediately closed and isolated the strainer. Upon investigation it was determined that local operations did not properly follow procedures to prepare the area for maintenance by turning off the power source and locking out the actuator. This allowed the controller to open an incorrect remote valve in error. All internal and external notifications were made. Osro arrived on site. Clean up activities continued for several days. All affected stone and soil was properly disposed of. All personnel were drug and alcohol tested. There were no injuries. No further remediation is needed.

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