HL incident on 2019-09-20 — TX

Operator
Valero Partners Operating Co. Llc
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-09-20 06:00
Report number
Location
TX
Narrative
Tank 1958 roof listed during an unusually heavy rain brought on by tropical storm imelda 2019. Crude oil surface onto the top of the tank roof through the tank roof seals.The tank roof realigned as the rainwater and crude oil released through the open rainwater roof drains. The crude oil and rainwater was contained inside valero's tank berm. Crude oil was recovered back into the tank and contaminated soil will be disposed in accordance with state and federal regulations. The tank was static during the rain storm. Valero initiated an incident investigation. After the crude oil was recovered the tank was inspected for integrity. No integrity issues were found during the inspection. Valero's incident investigation is currently ongoing. Tank 1958 has an external floating roof with dual articulated type roof drains with pivot master joints. Valero has taken this tank out of service on november 6, 2019 to assess the integrity of the roof drains. On december 5, 2019, valero completed the internal cleaning of the tank to assess the internal roof drains and replace all joints with new pivot masters. Upon visual inspection of the roof drain lines, it was determined that one of the support chains on the north drain line connecting the articulating joints was compromised. All pivot mater joints will be removed and sent to a third party for a pressure test and integrity assessment. The incident investigation will remain open until all inspection data of the roof drains is complete. 1/24/2020 cause was determined the support chain on the north drain line connecting the articulating joint was compromised. A split link connector spread apart and detached. Repaired the roof drain chain on the articulating joint by welding the split link.
Detailed record list
Report Received Date
2019-10-18 00:00:00
Iyear
2019
Report Number
20190318
Supplemental Number
33231
Report Type
Supplemental Final
Operator Id
Name
Valero Partners Operating Co. Llc
Operator Street Address
One Valero Way
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78249
Local Datetime
2019-09-20 06:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
86
Recovered Bbls
86
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-09-20 06:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Tank Was Already Static.
On Site Datetime
2019-09-20 06:00:00
Nrc Rpt Datetime
2019-09-20 09:07:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lucas Tank 1958
Segment Name
Lucas Tank 1958
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Lucas Tank Fa
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Roof/roof Seal
Tank Type
Atmospheric
Installation Year
1953
Material Involved
Material Other Than Carbon Steel
Material Details
Mechanical Shoe
Release Type
Other
Release Type Details
Tank Roof Listed
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
33062
Est Cost Other
143875
Est Cost Other Details
Environmental And Repairs
Prpty
176937
Accident Psig
4
Mop Psig
220
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was not associated with the pipeline. The tank was static.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Tank Roof Listed During An Unusually Heavy Rain. The Tank Roof Realigned As The Rainwater And Crude Oil Was Being Released Through The Open Rain Roof Drains.
Nf Extreme Weather Ind
Yes
Nf Tropical Storm Ind
Yes
Preparer Name
J**** T******
Preparer Title
Manager Regulatory Programs
Preparer Email
J************@v*****.com
Preparer Telephone
2103455145
Preparer Fax
2103706235
Prepared Date
2020-01-24 00:00:00
Authorizer Name
F*** H******
Authorizer Telephone
2013452000
Authorizer Title
Vice President Pipelines Terminals
Authorizer Email
F***********@v*****.com
Narrative
Tank 1958 roof listed during an unusually heavy rain brought on by tropical storm imelda 2019. Crude oil surface onto the top of the tank roof through the tank roof seals.The tank roof realigned as the rainwater and crude oil released through the open rainwater roof drains. The crude oil and rainwater was contained inside valero's tank berm. Crude oil was recovered back into the tank and contaminated soil will be disposed in accordance with state and federal regulations. The tank was static during the rain storm. Valero initiated an incident investigation. After the crude oil was recovered the tank was inspected for integrity. No integrity issues were found during the inspection. Valero's incident investigation is currently ongoing. Tank 1958 has an external floating roof with dual articulated type roof drains with pivot master joints. Valero has taken this tank out of service on november 6, 2019 to assess the integrity of the roof drains. On december 5, 2019, valero completed the internal cleaning of the tank to assess the internal roof drains and replace all joints with new pivot masters. Upon visual inspection of the roof drain lines, it was determined that one of the support chains on the north drain line connecting the articulating joints was compromised. All pivot mater joints will be removed and sent to a third party for a pressure test and integrity assessment. The incident investigation will remain open until all inspection data of the roof drains is complete. 1/24/2020 cause was determined the support chain on the north drain line connecting the articulating joint was compromised. A split link connector spread apart and detached. Repaired the roof drain chain on the articulating joint by welding the split link.
Report Received Date 2019-10-18 00:00:00
Iyear 2019
Report Number 20190318
Supplemental Number 33231
Report Type Supplemental Final
Operator Id 39105 PHMSA Enforcement
Name Valero Partners Operating Co. Llc
Operator Street Address One Valero Way
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78249
Local Datetime 2019-09-20 06:00:00
Location Latitude 29.995764 Google Maps OpenStreetMap
Location Longitude -94.077853 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 86
Recovered Bbls 86
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-09-20 06:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Tank Was Already Static.
On Site Datetime 2019-09-20 06:00:00
Nrc Rpt Datetime 2019-09-20 09:07:00
Nrc Rpt Num 1258768 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lucas Tank 1958
Segment Name Lucas Tank 1958
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Lucas Tank Fa
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Roof/roof Seal
Tank Type Atmospheric
Installation Year 1953
Material Involved Material Other Than Carbon Steel
Material Details Mechanical Shoe
Release Type Other
Release Type Details Tank Roof Listed
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 33062
Est Cost Other 143875
Est Cost Other Details Environmental And Repairs
Prpty 176937
Accident Psig 4
Mop Psig 220
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was not associated with the pipeline. The tank was static.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Other
Nf Other Details Tank Roof Listed During An Unusually Heavy Rain. The Tank Roof Realigned As The Rainwater And Crude Oil Was Being Released Through The Open Rain Roof Drains.
Nf Extreme Weather Ind Yes
Nf Tropical Storm Ind Yes
Preparer Name J**** T******
Preparer Title Manager Regulatory Programs
Preparer Email J************@v*****.com
Preparer Telephone 2103455145
Preparer Fax 2103706235
Prepared Date 2020-01-24 00:00:00
Authorizer Name F*** H******
Authorizer Telephone 2013452000
Authorizer Title Vice President Pipelines Terminals
Authorizer Email F***********@v*****.com
Narrative Tank 1958 roof listed during an unusually heavy rain brought on by tropical storm imelda 2019. Crude oil surface onto the top of the tank roof through the tank roof seals.The tank roof realigned as the rainwater and crude oil released through the open rainwater roof drains. The crude oil and rainwater was contained inside valero's tank berm. Crude oil was recovered back into the tank and contaminated soil will be disposed in accordance with state and federal regulations. The tank was static during the rain storm. Valero initiated an incident investigation. After the crude oil was recovered the tank was inspected for integrity. No integrity issues were found during the inspection. Valero's incident investigation is currently ongoing. Tank 1958 has an external floating roof with dual articulated type roof drains with pivot master joints. Valero has taken this tank out of service on november 6, 2019 to assess the integrity of the roof drains. On december 5, 2019, valero completed the internal cleaning of the tank to assess the internal roof drains and replace all joints with new pivot masters. Upon visual inspection of the roof drain lines, it was determined that one of the support chains on the north drain line connecting the articulating joints was compromised. All pivot mater joints will be removed and sent to a third party for a pressure test and integrity assessment. The incident investigation will remain open until all inspection data of the roof drains is complete. 1/24/2020 cause was determined the support chain on the north drain line connecting the articulating joint was compromised. A split link connector spread apart and detached. Repaired the roof drain chain on the articulating joint by welding the split link.

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