HL incident on 2019-09-20 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$700,000
Incident datetime
2019-09-20 19:10
Report number
Location
TX
Narrative
On 9/20/19 at approximately 1910, terminal operator noticed a gasoline odor near tank 28. During a field walk the employee discovered staining on the concrete ring wall and notified his supervisor. Emergency response team responded and confirmed that the staining was product coming from the tank. Proper agency notifications were made and the tank was removed from service pending an investigation into the cause of the release. A certified API 653 inspector came in and determined the cause of the leak to be a crack in the corner weld. The tank has been returned to service. Phmsa 48 hr update #: 1258944.
Detailed record list
Report Received Date
2019-10-18 00:00:00
Iyear
2019
Report Number
20190317
Supplemental Number
34776
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-09-20 19:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-09-20 19:10:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Idle At The Time Of Discovery.
On Site Datetime
2019-09-20 19:10:00
Nrc Rpt Datetime
2019-09-20 19:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Perth Amboy Terminal
Segment Name
Tank 28
Onshore State Abbreviation
Nj
Onshore Postal Code
08861
Onshore City Name
Perth Amboy
Onshore County Name
Middlesex
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Installation Year
1982
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3
Est Cost Prop Damage
700000
Est Cost Emergency
1000
Est Cost Environmental
32000
Est Cost Other
0
Prpty
733003
Accident Psig
14.7
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This did not occur during a control room operation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Corner Weld Crack
Eq Additional Other Ind
Yes
Eq Additional Other Details
Corner Weld Crack
Preparer Name
D******* S*******
Preparer Title
Director Of Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
713-725-0147
Preparer Fax
303-984-3048
Prepared Date
2021-01-28 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713-725-0147
Authorizer Title
Director Of Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 9/20/19 at approximately 1910, terminal operator noticed a gasoline odor near tank 28. During a field walk the employee discovered staining on the concrete ring wall and notified his supervisor. Emergency response team responded and confirmed that the staining was product coming from the tank. Proper agency notifications were made and the tank was removed from service pending an investigation into the cause of the release. A certified API 653 inspector came in and determined the cause of the leak to be a crack in the corner weld. The tank has been returned to service. Phmsa 48 hr update #: 1258944.
Report Received Date 2019-10-18 00:00:00
Iyear 2019
Report Number 20190317
Supplemental Number 34776
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-09-20 19:10:00
Location Latitude 40.523574 Google Maps OpenStreetMap
Location Longitude -74.252607 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-09-20 19:10:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Idle At The Time Of Discovery.
On Site Datetime 2019-09-20 19:10:00
Nrc Rpt Datetime 2019-09-20 19:59:00
Nrc Rpt Num 1258847 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Perth Amboy Terminal
Segment Name Tank 28
Onshore State Abbreviation Nj
Onshore Postal Code 08861
Onshore City Name Perth Amboy
Onshore County Name Middlesex
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Installation Year 1982
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3
Est Cost Prop Damage 700000
Est Cost Emergency 1000
Est Cost Environmental 32000
Est Cost Other 0
Prpty 733003
Accident Psig 14.7
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This did not occur during a control room operation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Corner Weld Crack
Eq Additional Other Ind Yes
Eq Additional Other Details Corner Weld Crack
Preparer Name D******* S*******
Preparer Title Director Of Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 713-725-0147
Preparer Fax 303-984-3048
Prepared Date 2021-01-28 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713-725-0147
Authorizer Title Director Of Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 9/20/19 at approximately 1910, terminal operator noticed a gasoline odor near tank 28. During a field walk the employee discovered staining on the concrete ring wall and notified his supervisor. Emergency response team responded and confirmed that the staining was product coming from the tank. Proper agency notifications were made and the tank was removed from service pending an investigation into the cause of the release. A certified API 653 inspector came in and determined the cause of the leak to be a crack in the corner weld. The tank has been returned to service. Phmsa 48 hr update #: 1258944.

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