HL incident on 2019-09-16 — TX

Operator
Exxonmobil Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100,000
Incident datetime
2019-09-16 06:50
Report number
Location
TX
Narrative
On the morning of september 16, 2019, local operating personnel discovered crude near the 16" meter skid at empco's webster station. The station was shutdown and isolated. The source of the crude was identified as internal corrosion on the bottom of a partially buried strainer. The site was cleaned up and restored and all spilled free product was recovered. A metallurgical analysis was performed and determined to be internal corrosion due to microbial induced corrosion. It was determined that, even though the strainer and associated piping was on the sites low point drain list for regular flushing, that the drain valve was clogged, preventing proper draining and flowing of the strainer. The strainer will be replaced with a new strainer and steps will be taken to verify that the sump is gaining during the low point drain flushing operations to assure flow through the strainer.
Detailed record list
Report Received Date
2019-10-15 00:00:00
Iyear
2019
Report Number
20190311
Supplemental Number
32824
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2019-09-16 06:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-09-16 06:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-09-16 06:54:00
Restart Datetime
2019-09-17 05:06:00
On Site Datetime
2019-09-16 06:50:00
Nrc Rpt Datetime
2019-09-16 08:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Webster Station
Segment Name
Ba 25, Webster To Baytown 16 Inch Crude Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77598
Onshore City Name
Webster
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Webster Stati
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
3
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
114
Est Cost Prop Damage
100000
Est Cost Emergency
500000
Est Cost Environmental
0
Est Cost Other
0
Prpty
600114
Accident Psig
10
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident did not involved occ.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Preparer Name
J** M*********
Preparer Title
Pipeline Safety Advisor
Preparer Email
J*****************@e*********.com
Preparer Telephone
832-624-6121
Prepared Date
2019-10-15 00:00:00
Authorizer Name
C******* B* H********
Authorizer Telephone
832-624-7920
Authorizer Title
Empco Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
On the morning of september 16, 2019, local operating personnel discovered crude near the 16" meter skid at empco's webster station. The station was shutdown and isolated. The source of the crude was identified as internal corrosion on the bottom of a partially buried strainer. The site was cleaned up and restored and all spilled free product was recovered. A metallurgical analysis was performed and determined to be internal corrosion due to microbial induced corrosion. It was determined that, even though the strainer and associated piping was on the sites low point drain list for regular flushing, that the drain valve was clogged, preventing proper draining and flowing of the strainer. The strainer will be replaced with a new strainer and steps will be taken to verify that the sump is gaining during the low point drain flushing operations to assure flow through the strainer.
Report Received Date 2019-10-15 00:00:00
Iyear 2019
Report Number 20190311
Supplemental Number 32824
Report Type Supplemental Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2019-09-16 06:50:00
Location Latitude 29.5208806 Google Maps OpenStreetMap
Location Longitude -95.1061667 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 1.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-09-16 06:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-09-16 06:54:00
Restart Datetime 2019-09-17 05:06:00
On Site Datetime 2019-09-16 06:50:00
Nrc Rpt Datetime 2019-09-16 08:00:00
Nrc Rpt Num 1258346 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Webster Station
Segment Name Ba 25, Webster To Baytown 16 Inch Crude Line
Onshore State Abbreviation Tx
Onshore Postal Code 77598
Onshore City Name Webster
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Webster Stati
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 3
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 114
Est Cost Prop Damage 100000
Est Cost Emergency 500000
Est Cost Environmental 0
Est Cost Other 0
Prpty 600114
Accident Psig 10
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident did not involved occ.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Preparer Name J** M*********
Preparer Title Pipeline Safety Advisor
Preparer Email J*****************@e*********.com
Preparer Telephone 832-624-6121
Prepared Date 2019-10-15 00:00:00
Authorizer Name C******* B* H********
Authorizer Telephone 832-624-7920
Authorizer Title Empco Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative On the morning of september 16, 2019, local operating personnel discovered crude near the 16" meter skid at empco's webster station. The station was shutdown and isolated. The source of the crude was identified as internal corrosion on the bottom of a partially buried strainer. The site was cleaned up and restored and all spilled free product was recovered. A metallurgical analysis was performed and determined to be internal corrosion due to microbial induced corrosion. It was determined that, even though the strainer and associated piping was on the sites low point drain list for regular flushing, that the drain valve was clogged, preventing proper draining and flowing of the strainer. The strainer will be replaced with a new strainer and steps will be taken to verify that the sump is gaining during the low point drain flushing operations to assure flow through the strainer.

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