HL incident on 2019-09-18 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150,000
Incident datetime
2019-09-18 07:25
Report number
Location
PA
Narrative
On september 18, 2019 at 07:25 a.M., dearborn terminal operator discovered jet fuel in the secondary containment (dike area) of tank 1. The spill was discovered to have originated from a vent on a non-DOT jurisdictional tank (1a) connected to the jet fuel filter system. Internal and external notifications were made. An osro assisted in cleanup efforts. The estimated release volume is 75 barrels, all of which was recovered. The root cause of the event was determined to be human error. Employee failed to follow lock out tag out procedures which resulted in ball valves in the jet fuel filter system left in the partially open position. Employees involved in the incident were re-trained in applicable procedures.
Detailed record list
Report Received Date
2019-10-11 00:00:00
Iyear
2019
Report Number
20190308
Supplemental Number
33217
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2019-09-18 07:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
75
Recovered Bbls
75
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-09-18 07:25:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-09-18 07:42:00
Restart Datetime
2019-09-18 16:30:00
On Site Datetime
2019-09-18 09:50:00
Nrc Rpt Datetime
2019-09-18 10:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dearborn Terminal
Segment Name
Dearborn Terminal - Betit
Onshore State Abbreviation
Mi
Onshore Postal Code
48180
Onshore City Name
Taylor
Onshore County Name
Wayne
Designated Location
Milepost/valve Station
Designated Name
Dearborn Term
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Jet Fuel Filter System
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1300
Est Cost Prop Damage
150000
Est Cost Emergency
24000
Est Cost Environmental
0
Est Cost Other
21000
Est Cost Other Details
Buckeye Labor And Travel
Prpty
196300
Accident Psig
6
Mop Psig
150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Valve In Wrong Position That Resulted In Tank Overflow
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D***** R******
Preparer Title
District Compiance Specialist
Preparer Email
D*******@b******.com
Preparer Telephone
412-216-2864
Preparer Fax
412-264-1433
Prepared Date
2020-01-22 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On september 18, 2019 at 07:25 a.M., dearborn terminal operator discovered jet fuel in the secondary containment (dike area) of tank 1. The spill was discovered to have originated from a vent on a non-DOT jurisdictional tank (1a) connected to the jet fuel filter system. Internal and external notifications were made. An osro assisted in cleanup efforts. The estimated release volume is 75 barrels, all of which was recovered. The root cause of the event was determined to be human error. Employee failed to follow lock out tag out procedures which resulted in ball valves in the jet fuel filter system left in the partially open position. Employees involved in the incident were re-trained in applicable procedures.
Report Received Date 2019-10-11 00:00:00
Iyear 2019
Report Number 20190308
Supplemental Number 33217
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2019-09-18 07:20:00
Location Latitude 42.244489 Google Maps OpenStreetMap
Location Longitude -83.302939 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 75
Recovered Bbls 75
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-09-18 07:25:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-09-18 07:42:00
Restart Datetime 2019-09-18 16:30:00
On Site Datetime 2019-09-18 09:50:00
Nrc Rpt Datetime 2019-09-18 10:27:00
Nrc Rpt Num 1258568 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Dearborn Terminal
Segment Name Dearborn Terminal - Betit
Onshore State Abbreviation Mi
Onshore Postal Code 48180
Onshore City Name Taylor
Onshore County Name Wayne
Designated Location Milepost/valve Station
Designated Name Dearborn Term
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Jet Fuel Filter System
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1300
Est Cost Prop Damage 150000
Est Cost Emergency 24000
Est Cost Environmental 0
Est Cost Other 21000
Est Cost Other Details Buckeye Labor And Travel
Prpty 196300
Accident Psig 6
Mop Psig 150
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Valve In Wrong Position That Resulted In Tank Overflow
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D***** R******
Preparer Title District Compiance Specialist
Preparer Email D*******@b******.com
Preparer Telephone 412-216-2864
Preparer Fax 412-264-1433
Prepared Date 2020-01-22 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On september 18, 2019 at 07:25 a.M., dearborn terminal operator discovered jet fuel in the secondary containment (dike area) of tank 1. The spill was discovered to have originated from a vent on a non-DOT jurisdictional tank (1a) connected to the jet fuel filter system. Internal and external notifications were made. An osro assisted in cleanup efforts. The estimated release volume is 75 barrels, all of which was recovered. The root cause of the event was determined to be human error. Employee failed to follow lock out tag out procedures which resulted in ball valves in the jet fuel filter system left in the partially open position. Employees involved in the incident were re-trained in applicable procedures.

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