HL incident on 2019-09-11 — CO

Operator
Tallgrass Pony Express Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2019-09-11 10:02
Report number
Location
CO
Narrative
On september 11th, 2019 at approx. 0946 mst, an operations employee was performing a 22" pig launch of a pig preloaded the day before. The employee missed the alarm notification call initiated by the lakewood, co occ. Upon seeing the missed call and returning the call occ informed the operations employee that the sump was at high high and proceeded back to the sump. Upon arriving at the sump at approx. 1002 mst, the operations employee noticed that the t-7200 sump was overflowing and called occ at 1003 mst and told them to shut down the station. The operations employee then went to investigate the 22" pig launcher and saw that valve #1407 was closed but valve #1407b was open. The operations employee then closed valve #1407b and isolated the source of oil to t-7200 sump. At approximately 1006 mst the operations employee notified the sterling operations supervisor that there was oil on the ground and proceeded to initiate containment and cleanup operations. Cleanup commenced approximately 1115 mt.
Detailed record list
Report Received Date
2019-10-07 00:00:00
Iyear
2019
Report Number
20190304
Supplemental Number
32828
Report Type
Supplemental Final
Operator Id
Name
Tallgrass Pony Express Pipeline, Llc
Operator Street Address
370 Van Gordon St.
Operator City Name
Lakewood
Operator State Abbreviation
CO
Operator Postal Code
80228
Local Datetime
2019-09-11 10:02:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-09-11 10:02:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-09-11 10:03:00
Restart Datetime
2019-09-11 12:15:00
On Site Datetime
2019-09-11 10:02:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Sterling Terminal
Segment Name
Sterling Terminal
Onshore State Abbreviation
Co
Onshore Postal Code
80751
Onshore City Name
Not Within A Municipality
Onshore County Name
Logan
Designated Location
Milepost/valve Station
Designated Name
Sterling
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
850
Est Cost Prop Damage
15000
Est Cost Emergency
20000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
55850
Accident Psig
163
Mop Psig
270
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was a result of improper field operation (unrelated to control room)
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
B*** A*******
Preparer Title
Compliance Engineer
Preparer Email
B************@t****************.com
Preparer Telephone
303-763-3112
Prepared Date
2019-10-16 00:00:00
Authorizer Name
B*** A*******
Authorizer Telephone
303-763-3112
Authorizer Title
Compliance Engineer
Authorizer Email
B************@t****************.com
Narrative
On september 11th, 2019 at approx. 0946 mst, an operations employee was performing a 22" pig launch of a pig preloaded the day before. The employee missed the alarm notification call initiated by the lakewood, co occ. Upon seeing the missed call and returning the call occ informed the operations employee that the sump was at high high and proceeded back to the sump. Upon arriving at the sump at approx. 1002 mst, the operations employee noticed that the t-7200 sump was overflowing and called occ at 1003 mst and told them to shut down the station. The operations employee then went to investigate the 22" pig launcher and saw that valve #1407 was closed but valve #1407b was open. The operations employee then closed valve #1407b and isolated the source of oil to t-7200 sump. At approximately 1006 mst the operations employee notified the sterling operations supervisor that there was oil on the ground and proceeded to initiate containment and cleanup operations. Cleanup commenced approximately 1115 mt.
Report Received Date 2019-10-07 00:00:00
Iyear 2019
Report Number 20190304
Supplemental Number 32828
Report Type Supplemental Final
Operator Id 39043 PHMSA Enforcement
Name Tallgrass Pony Express Pipeline, Llc
Operator Street Address 370 Van Gordon St.
Operator City Name Lakewood
Operator State Abbreviation CO
Operator Postal Code 80228
Local Datetime 2019-09-11 10:02:00
Location Latitude 40.652947 Google Maps OpenStreetMap
Location Longitude -103.033132 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-09-11 10:02:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-09-11 10:03:00
Restart Datetime 2019-09-11 12:15:00
On Site Datetime 2019-09-11 10:02:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Sterling Terminal
Segment Name Sterling Terminal
Onshore State Abbreviation Co
Onshore Postal Code 80751
Onshore City Name Not Within A Municipality
Onshore County Name Logan
Designated Location Milepost/valve Station
Designated Name Sterling
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year 2015
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 850
Est Cost Prop Damage 15000
Est Cost Emergency 20000
Est Cost Environmental 20000
Est Cost Other 0
Prpty 55850
Accident Psig 163
Mop Psig 270
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was a result of improper field operation (unrelated to control room)
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name B*** A*******
Preparer Title Compliance Engineer
Preparer Email B************@t****************.com
Preparer Telephone 303-763-3112
Prepared Date 2019-10-16 00:00:00
Authorizer Name B*** A*******
Authorizer Telephone 303-763-3112
Authorizer Title Compliance Engineer
Authorizer Email B************@t****************.com
Narrative On september 11th, 2019 at approx. 0946 mst, an operations employee was performing a 22" pig launch of a pig preloaded the day before. The employee missed the alarm notification call initiated by the lakewood, co occ. Upon seeing the missed call and returning the call occ informed the operations employee that the sump was at high high and proceeded back to the sump. Upon arriving at the sump at approx. 1002 mst, the operations employee noticed that the t-7200 sump was overflowing and called occ at 1003 mst and told them to shut down the station. The operations employee then went to investigate the 22" pig launcher and saw that valve #1407 was closed but valve #1407b was open. The operations employee then closed valve #1407b and isolated the source of oil to t-7200 sump. At approximately 1006 mst the operations employee notified the sterling operations supervisor that there was oil on the ground and proceeded to initiate containment and cleanup operations. Cleanup commenced approximately 1115 mt.

All rights reserved. Copyright © by ClearPHMSA